Differences between revisions 128 and 139 (spanning 11 versions)
Revision 128 as of 2017-03-03 13:29:51
Size: 1305
Editor: MarkBarton
Comment:
Revision 139 as of 2017-04-27 15:53:11
Size: 1534
Editor: MarkBarton
Comment:
Deletions are marked like this. Additions are marked like this.
Line 7: Line 7:
At Kamioka (Mark, Fabian, Enzo, Hirata-san):
 * With help from Kokeyama-san and Miyakawa-san, we debugged a problem with the real-time model freezing, which turned out to be the IO chassis shutting down because of brownout condition from an overloaded AC circuit. A combination of extra boxes added to the rack, plus surge current from the air shower could draw the full 20 A limit of the circuit. Awai-san ran a cable to a separate circuit and we moved the IO chassis onto that.
 * We got the stepper motor cabling and driver working, and tested the BF fishing rod stepper motor.
 * We got the LVDT cabling, driver and associated parts of the real-time model working.
 * We found all the parts for the SF and the SF section of the security structure, and prepared the SF. However we then removed the Cu ring from the top cap for recleaning.
 *
At Kamioka (Mark, Fabian, Enzo, Perry, Hirata-san):

 * Craned in the PI.
 * Assembled the thrust bearing holder that receives the PI-SF rod. (It originally had a burr that prevented the bearing from seating properly, and so required filing and re-cleaning.)
 * Hooked the SF and lowered the jacks under the SF to suspend the SF/... section.
 * The top filter rose when unlocked, and required about 1.8 kg to send it back down. Therefore we may be OK - the top filter seems to have about 8 kg more capacity than as measured by G&M. The hex cable clamp (≈0.25 kg) and the cables between the PI and SF still have to be added, but we can get an extra 3 kg by removing one of the three Cu damper segments (and rearranging the other two).
 * Built and installed three LBB blade units.
 * Kept debugging the SF LVDT. We repaired several broken wires, but it's still not behaving correctly.
Line 14: Line 17:
Next week:
 * Everyone (Mark, Fabian, Enzo, Hirata-san) at Kamioka, Monday-Thursday.
 * Work on electronics, possibly suspend and weigh BF.
Week after next:
 * Everyone (Mark, Fabian, Enzo, Hirata-san) at Kamioka, Monday-Friday.
 * Add SF and suspend BF.
For more detail, see [[KAGRA/Subgroups/VIS/TypeB/ToDo]].

Week of 5/1:
 * No activity (Golden Week).

Week of 5/8:
 * Work from Tuesday.
 * Remove PI temporarily.
 * Add magnets to upper SF damper ring.
 * Reinstall PI with damper ring.
 * Reinstall PI-SF rod, this time with hex cable clamp.
 * Install PI yaw stepper.
 * Wire up PI yaw and vertical steppers.
 * Route cables from SF to PI (may involve removing part of Cu damper).

Scraps of text for incorporation in the VIS Meeting Minutes

KAGRA/Subgroups/VIS/MeetingNAOJ

Type B (Mark)

Past week report

At Kamioka (Mark, Fabian, Enzo, Perry, Hirata-san):

  • Craned in the PI.
  • Assembled the thrust bearing holder that receives the PI-SF rod. (It originally had a burr that prevented the bearing from seating properly, and so required filing and re-cleaning.)
  • Hooked the SF and lowered the jacks under the SF to suspend the SF/... section.
  • The top filter rose when unlocked, and required about 1.8 kg to send it back down. Therefore we may be OK - the top filter seems to have about 8 kg more capacity than as measured by G&M. The hex cable clamp (≈0.25 kg) and the cables between the PI and SF still have to be added, but we can get an extra 3 kg by removing one of the three Cu damper segments (and rearranging the other two).

  • Built and installed three LBB blade units.
  • Kept debugging the SF LVDT. We repaired several broken wires, but it's still not behaving correctly.

Plan for coming weeks

For more detail, see KAGRA/Subgroups/VIS/TypeB/ToDo.

Week of 5/1:

  • No activity (Golden Week).

Week of 5/8:

  • Work from Tuesday.
  • Remove PI temporarily.
  • Add magnets to upper SF damper ring.
  • Reinstall PI with damper ring.
  • Reinstall PI-SF rod, this time with hex cable clamp.
  • Install PI yaw stepper.
  • Wire up PI yaw and vertical steppers.
  • Route cables from SF to PI (may involve removing part of Cu damper).

KAGRA/Subgroups/VIS/TypeB/Minutes (last edited 2022-10-28 10:02:46 by fabian.arellano)