Differences between revisions 136 and 140 (spanning 4 versions)
Revision 136 as of 2017-04-07 13:21:26
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Editor: MarkBarton
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Revision 140 as of 2017-04-27 19:31:10
Size: 2348
Editor: MarkBarton
Comment:
Deletions are marked like this. Additions are marked like this.
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 * We set things up again after the floor coating work.
 * We moved the PI into the second floor of the cleanbooth:
  * We cleared a path for the forklift (moving the portable cleanroom, worktable, power cables, vacuum pumps and other obstacles).
  * We got Saito-sensei to move the PI to the +Y side of the cleanbooth.
  * We washed and cling-wrapped a pallet.
  * We got Miyoki-san to disconnect the cables and curtain blocking the crane slot (and reconnect them afterwards).
  * We added some temporary crossbars in the top of the assembly frame and stored the SF cap on them to get it out of the way.
  * We craned in the pallet and set it up to bridge three floor joists.
  * We craned in the PI using Saito-san's adapter.
   * We couldn't find the original screws for the three PI transport plates so we substituted some others - fortunately there was no galling.
   * We had to connect the adapter to the crane with a sling because the ring for the hook was slightly too small).
 * We did a lot of cabling work:
  * We routed all the BF cables over the BF cap, up through the cable clamp on the SF-BF rod and up to the SF. (We had to redo a few because the Type 3 cable was at the flange end instead of the Type 1.)
  * We connected up the SF LVDT and FR stepper.
  * We started on rebalancing the BF (which had been perturbed by the weight and tension of all the cables). We got it rather better, but it needs more work.
  * We made another batch of anti-feedthrough adapters.

 * We craned in the PI.
 * We assembled the thrust bearing holder that receives the PI-SF rod. (The recess for the bearing was very slightly too small and had a burr near a retaining screw hole that prevented the bearing from seating properly, and so it required filing and re-cleaning.)
 * We hooked the SF and lowered the jacks under the SF to suspend the SF/... section.
 * The top filter rose when unlocked, and required about 1.8 kg to send it back down. Therefore we may be OK - the top filter seems to have about 8 kg more capacity than as measured by G&M. The hex cable clamp (≈0.25 kg) and the cables between the PI and SF still have to be added, but we can get an extra 3 kg by removing one of the three Cu damper segments (and rearranging the other two).
 * Hirata-san built and installed three LBB blade units.
 * Enzo kept debugging the SF LVDT. We repaired several broken wires, but it's still not behaving correctly. We suspect the ordering of the three coils (input output and excitation) may not be right. If so, we should be able to fix it with an adapter cable without removing the SF cap.
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Week of 4/10:
 * Hirata-san does scissor lift training 4/10.
 * Perry in Tokyo 4/10.
 * Debug/fix dead OSEM channel, TM-H4.
 * Debug BF/SF LVDTs.
 * Adjust BF pitch/roll.
 * Do TF from SF LVDT actuation.
 * Install temporary ballast mass in SF.
 * Lift SF/BF/... section and check total weight and SF balance.
 * Continue swap of PI LVDT connectors (female->male)
 * Start preparing LBB spring units.
 * Install pico drivers in rack, create MEDM interface (with Miyo-kun), and undo temporary connection of picos to old controller and joystick.
Week of 4/17:
 * Crane in PI.
 * Connect SF/BF... section.
 * Temporarily remove PI and adjust SF ballast if necessary.
Week of 5/1:
 * No activity (Golden Week).

Week of 5/8:
 * Commence work Tuesday 5/9.
 * Remove PI temporarily.
 * Continue debugging SF LVDT (removing cap if necessary).
 * Investigate possible mis-alignment between the tips of the LBB blades and the holes for the rods going down to the damper ring.
 * Add magnets to upper SF damper ring.
 * Reinstall PI, this time with rods and damper ring.
 * Reinstall PI-SF rod, this time with hex cable clamp.
 * Install PI yaw stepper.
 * Wire up PI yaw stepper and vertical fishing-rod steppers.
 * Route cables from SF to PI (may involve removing part of Cu damper).

Week of 5/15:
 * Enzo from Tuesday 5/16 (driving test), rest of team from Monday.
 * Prepare for PR2 bellows removal on 5/15 (move table with tools).
 * Wire up PI horizontal LVDTs and steppers.
 * Install geophones.
 * Unlock IP, re-level PI to center PI, add arc weights as required.

Scraps of text for incorporation in the VIS Meeting Minutes

KAGRA/Subgroups/VIS/MeetingNAOJ

Type B (Mark)

Past week report

At Kamioka (Mark, Fabian, Enzo, Perry, Hirata-san):

  • We craned in the PI.
  • We assembled the thrust bearing holder that receives the PI-SF rod. (The recess for the bearing was very slightly too small and had a burr near a retaining screw hole that prevented the bearing from seating properly, and so it required filing and re-cleaning.)
  • We hooked the SF and lowered the jacks under the SF to suspend the SF/... section.
  • The top filter rose when unlocked, and required about 1.8 kg to send it back down. Therefore we may be OK - the top filter seems to have about 8 kg more capacity than as measured by G&M. The hex cable clamp (≈0.25 kg) and the cables between the PI and SF still have to be added, but we can get an extra 3 kg by removing one of the three Cu damper segments (and rearranging the other two).

  • Hirata-san built and installed three LBB blade units.
  • Enzo kept debugging the SF LVDT. We repaired several broken wires, but it's still not behaving correctly. We suspect the ordering of the three coils (input output and excitation) may not be right. If so, we should be able to fix it with an adapter cable without removing the SF cap.

Plan for coming weeks

For more detail, see KAGRA/Subgroups/VIS/TypeB/ToDo.

Week of 5/1:

  • No activity (Golden Week).

Week of 5/8:

  • Commence work Tuesday 5/9.
  • Remove PI temporarily.
  • Continue debugging SF LVDT (removing cap if necessary).
  • Investigate possible mis-alignment between the tips of the LBB blades and the holes for the rods going down to the damper ring.
  • Add magnets to upper SF damper ring.
  • Reinstall PI, this time with rods and damper ring.
  • Reinstall PI-SF rod, this time with hex cable clamp.
  • Install PI yaw stepper.
  • Wire up PI yaw stepper and vertical fishing-rod steppers.
  • Route cables from SF to PI (may involve removing part of Cu damper).

Week of 5/15:

  • Enzo from Tuesday 5/16 (driving test), rest of team from Monday.
  • Prepare for PR2 bellows removal on 5/15 (move table with tools).
  • Wire up PI horizontal LVDTs and steppers.
  • Install geophones.
  • Unlock IP, re-level PI to center PI, add arc weights as required.

KAGRA/Subgroups/VIS/TypeB/Minutes (last edited 2022-10-28 10:02:46 by fabian.arellano)