Differences between revisions 136 and 154 (spanning 18 versions)
Revision 136 as of 2017-04-07 13:21:26
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Revision 154 as of 2017-06-09 13:29:51
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Deletions are marked like this. Additions are marked like this.
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At Kamioka (Mark, Fabian, Enzo, Perry, Hirata-san):
 * We set things up again after the floor coating work.
 * We moved the PI into the second floor of the cleanbooth:
  * We cleared a path for the forklift (moving the portable cleanroom, worktable, power cables, vacuum pumps and other obstacles).
  * We got Saito-sensei to move the PI to the +Y side of the cleanbooth.
  * We washed and cling-wrapped a pallet.
  * We got Miyoki-san to disconnect the cables and curtain blocking the crane slot (and reconnect them afterwards).
  * We added some temporary crossbars in the top of the assembly frame and stored the SF cap on them to get it out of the way.
  * We craned in the pallet and set it up to bridge three floor joists.
  * We craned in the PI using Saito-san's adapter.
   * We couldn't find the original screws for the three PI transport plates so we substituted some others - fortunately there was no galling.
   * We had to connect the adapter to the crane with a sling because the ring for the hook was slightly too small).
 * We did a lot of cabling work:
  * We routed all the BF cables over the BF cap, up through the cable clamp on the SF-BF rod and up to the SF. (We had to redo a few because the Type 3 cable was at the flange end instead of the Type 1.)
  * We connected up the SF LVDT and FR stepper.
  * We started on rebalancing the BF (which had been perturbed by the weight and tension of all the cables). We got it rather better, but it needs more work.
  * We made another batch of anti-feedthrough adapters.
At Kamioka (Mark, Fabian, Enzo, Hirata-san):
 * Hirata-san and Mark reversed the support ring for the LBB damper to match the reversed suspension.
 * Hirata-san did a trial assembly of the magnet ring for the LLB damper and placed magnets on it with the template.
 * Hirata-san and Mark put the base pieces for the Cu ring in the chamber. However it turns out that the holes for attaching the joint pieces are incompletely threaded and we will have to run a tap through them.
 * We tested the geophones. At first one didn't work at all. This turned out to be a broken wire in one of the in-vacuum adapter cables. For the test we replaced the adapter with an old-style one (and removed the matching descrambler). A second geophone mostly works but saturates at a suspiciously low number of counts at the ADC (2000 instead of 20000).
 * We tested the PI horizontal LVDTs. The #1 (H2) one works but cable swaps showed that #0 and #2 have issues both at the tank end and at the card.
 * We decided on a final location for the stepper and pico drivers on the second floor. We moved the cables for the stepper drivers (using the outside cable trays) and laid new LAN and AC cables for the picos.
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Week of 4/10:
 * Hirata-san does scissor lift training 4/10.
 * Perry in Tokyo 4/10.
 * Debug/fix dead OSEM channel, TM-H4.
 * Debug BF/SF LVDTs.
 * Adjust BF pitch/roll.
 * Do TF from SF LVDT actuation.
 * Install temporary ballast mass in SF.
 * Lift SF/BF/... section and check total weight and SF balance.
 * Continue swap of PI LVDT connectors (female->male)
 * Start preparing LBB spring units.
 * Install pico drivers in rack, create MEDM interface (with Miyo-kun), and undo temporary connection of picos to old controller and joystick.
Week of 4/17:
 * Crane in PI.
 * Connect SF/BF... section.
 * Temporarily remove PI and adjust SF ballast if necessary.
 
Week of 6/6:
 * Cabling:
  * Finish moving in-air cabling to match feedthrough positions.
  * Cable and test PI vertical LVDT.
  * Calibrate PI vertical LVDT.
  * Set yoke on PI vertical LVDT (if necessary).
  * Cable and test PI yaw stepper.
  * Cable and test PI vertical stepper.
  * Cable and test PI horizontal steppers.
  * Cable and test PI horizontal LVDTs.
  * Calibrate PI horizontal LVDTs.

Week of 6/12:
 * Remove -Y flange cover, replace with cloth cover (or foil).
 * Prepare LBB.
  * Wipe LBB.
  * Loosen or remove LBB hold-down bolts.
  * Attach LBB outriggers and rod receptacles.
  * Lay out slings for LBB damper rings.
 * Prepare LBB damper support.
  * Install rods for LBB magnet ring.
  * Install safety rods for LBB Cu ring.
 * Prepare LBB Cu ring.
  * Pass into tank.
  * Reassemble on top of slings.
  * Lay down spacers to protect magnets (in next step).
 * Prepare LBB magnet ring.
  * Assemble temporarily.
  * Attach magnets with template.
  * Disassemble.
  * Pass into tank.
  * Reassemble on top of Cu ring.
 * Install LBB damper.
  * Pass sling ends through loops to bind LBB damper rings.
  * Remove vacuum tank lid and ring.
  * Crane rings up to install height, hook LBB magnet ring and support LBB Cu ring by TBD method.
 * Crane suspension into tank.
 * Hook LBB Cu ring.
 * Hook LBB.
 * Crane vacuum tank lid+ring black on.
 * Remove vacuum tank lid (only).
 * Remove port covers where feedthroughs will go, move feedthroughs from assembly frame and install on vacuum tank ring.
 * Cabling, cabling, cabling.

Scraps of text for incorporation in the VIS Meeting Minutes

KAGRA/Subgroups/VIS/MeetingNAOJ

Type B (Mark)

Past week report

At Kamioka (Mark, Fabian, Enzo, Hirata-san):

  • Hirata-san and Mark reversed the support ring for the LBB damper to match the reversed suspension.
  • Hirata-san did a trial assembly of the magnet ring for the LLB damper and placed magnets on it with the template.
  • Hirata-san and Mark put the base pieces for the Cu ring in the chamber. However it turns out that the holes for attaching the joint pieces are incompletely threaded and we will have to run a tap through them.
  • We tested the geophones. At first one didn't work at all. This turned out to be a broken wire in one of the in-vacuum adapter cables. For the test we replaced the adapter with an old-style one (and removed the matching descrambler). A second geophone mostly works but saturates at a suspiciously low number of counts at the ADC (2000 instead of 20000).
  • We tested the PI horizontal LVDTs. The #1 (H2) one works but cable swaps showed that #0 and #2 have issues both at the tank end and at the card.
  • We decided on a final location for the stepper and pico drivers on the second floor. We moved the cables for the stepper drivers (using the outside cable trays) and laid new LAN and AC cables for the picos.

Plan for coming weeks

For more detail, see KAGRA/Subgroups/VIS/TypeB/ToDo.

Week of 6/6:

  • Cabling:
    • Finish moving in-air cabling to match feedthrough positions.
    • Cable and test PI vertical LVDT.
    • Calibrate PI vertical LVDT.
    • Set yoke on PI vertical LVDT (if necessary).
    • Cable and test PI yaw stepper.
    • Cable and test PI vertical stepper.
    • Cable and test PI horizontal steppers.
    • Cable and test PI horizontal LVDTs.
    • Calibrate PI horizontal LVDTs.

Week of 6/12:

  • Remove -Y flange cover, replace with cloth cover (or foil).
  • Prepare LBB.
    • Wipe LBB.
    • Loosen or remove LBB hold-down bolts.
    • Attach LBB outriggers and rod receptacles.
    • Lay out slings for LBB damper rings.
  • Prepare LBB damper support.
    • Install rods for LBB magnet ring.
    • Install safety rods for LBB Cu ring.
  • Prepare LBB Cu ring.
    • Pass into tank.
    • Reassemble on top of slings.
    • Lay down spacers to protect magnets (in next step).
  • Prepare LBB magnet ring.
    • Assemble temporarily.
    • Attach magnets with template.
    • Disassemble.
    • Pass into tank.
    • Reassemble on top of Cu ring.
  • Install LBB damper.
    • Pass sling ends through loops to bind LBB damper rings.
    • Remove vacuum tank lid and ring.
    • Crane rings up to install height, hook LBB magnet ring and support LBB Cu ring by TBD method.
  • Crane suspension into tank.
  • Hook LBB Cu ring.
  • Hook LBB.
  • Crane vacuum tank lid+ring black on.
  • Remove vacuum tank lid (only).
  • Remove port covers where feedthroughs will go, move feedthroughs from assembly frame and install on vacuum tank ring.
  • Cabling, cabling, cabling.

KAGRA/Subgroups/VIS/TypeB/Minutes (last edited 2022-10-28 10:02:46 by fabian.arellano)