1534
Comment:
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2949
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Deletions are marked like this. | Additions are marked like this. |
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At Kamioka (Mark, Fabian, Enzo, Perry, Hirata-san): * Craned in the PI. * Assembled the thrust bearing holder that receives the PI-SF rod. (It originally had a burr that prevented the bearing from seating properly, and so required filing and re-cleaning.) * Hooked the SF and lowered the jacks under the SF to suspend the SF/... section. * The top filter rose when unlocked, and required about 1.8 kg to send it back down. Therefore we may be OK - the top filter seems to have about 8 kg more capacity than as measured by G&M. The hex cable clamp (≈0.25 kg) and the cables between the PI and SF still have to be added, but we can get an extra 3 kg by removing one of the three Cu damper segments (and rearranging the other two). * Built and installed three LBB blade units. * Kept debugging the SF LVDT. We repaired several broken wires, but it's still not behaving correctly. |
At Kamioka (Mark, Fabian, Enzo, Hirata-san): * Hirata-san and Sekine-san moved the tank lid and service port ring to the pallet with the crane and covered the open tank with the spare clean bag. * Hirata-san and Mark got the LBB damper rings assembled and installed. A joint part for the Cu ring needed to have holes enlarged because the hole pattern did not quite match that on the half-ring. The magnet ring is hanging in the chamber and the Cu ring is attached below it with clamps, ready to receive the rods that will hang down from the PI. * Hirata-san recounted all the unused cables. * Hirata-san installed the outrigger parts on the LBB, which will receive the rods coming down from the damper ring. * Enzo and Mark tested all the stepper motors. * Enzo and Mark debugged the PI horizontal LVDTs. One LVDT had a flaky connection and one card in the LVDT driver had three dead channels. Enzo created a fully working driver using parts from another driver that also had a faulty card. * Fabian adjusted the ballast mass on the SF to get good pitch/roll/vertical adjustment and attached it with screws. * Fabian set up the optical lever again (the PR2 team had repossessed the breadboard we had been using but Akutsu-san supplied another one). * Enzo and Mark tested the pico motors. The software is very unreliable, but we we able to confirm that the IM pitch pico works. * The whole team wrapped items and shut down equipment ahead of the power outage. |
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Week of 5/1: * No activity (Golden Week). Week of 5/8: * Work from Tuesday. * Remove PI temporarily. * Add magnets to upper SF damper ring. * Reinstall PI with damper ring. * Reinstall PI-SF rod, this time with hex cable clamp. * Install PI yaw stepper. * Wire up PI yaw and vertical steppers. * Route cables from SF to PI (may involve removing part of Cu damper). |
Week of 6/12: * Cabling: * Debug/fix PI vertical LVDTs #0 and #2. * Calibrate PI vertical LVDT. * Debug/fix geophone #1. * Set yoke on PI vertical LVDT (if necessary). * Cable and test PI yaw stepper. * Cable and test PI vertical stepper. * Cable and test PI horizontal steppers. * Cable and test PI horizontal LVDTs. * Calibrate PI horizontal LVDTs. * Prepare LBB. * Attach LBB outriggers and rod receptacles. * Prepare LBB Cu ring. * Remove from tank, fix incompletely threaded holes, reinstall in tank. * Lay down spacers to protect magnets (in next step). * Prepare LBB magnet ring. * Disassemble. * Pass pieces into tank. * Reassemble on top of Cu ring. * Install LBB damper. * Bind LBB damper rings together with slings. * Remove vacuum tank lid and ring. * Crane rings up to install height, hook LBB magnet ring and support LBB Cu ring by TBD method. * Crane suspension into tank. * Hook LBB Cu ring. * Hook LBB. * Crane vacuum tank lid+ring black on. * Remove vacuum tank lid (only). * Remove port covers where feedthroughs will go, move feedthroughs from assembly frame and install on vacuum tank ring. * Reconnect in-air cables. |
Scraps of text for incorporation in the VIS Meeting Minutes
KAGRA/Subgroups/VIS/MeetingNAOJ
Type B (Mark)
Past week report
At Kamioka (Mark, Fabian, Enzo, Hirata-san):
- Hirata-san and Sekine-san moved the tank lid and service port ring to the pallet with the crane and covered the open tank with the spare clean bag.
- Hirata-san and Mark got the LBB damper rings assembled and installed. A joint part for the Cu ring needed to have holes enlarged because the hole pattern did not quite match that on the half-ring. The magnet ring is hanging in the chamber and the Cu ring is attached below it with clamps, ready to receive the rods that will hang down from the PI.
- Hirata-san recounted all the unused cables.
- Hirata-san installed the outrigger parts on the LBB, which will receive the rods coming down from the damper ring.
- Enzo and Mark tested all the stepper motors.
- Enzo and Mark debugged the PI horizontal LVDTs. One LVDT had a flaky connection and one card in the LVDT driver had three dead channels. Enzo created a fully working driver using parts from another driver that also had a faulty card.
- Fabian adjusted the ballast mass on the SF to get good pitch/roll/vertical adjustment and attached it with screws.
- Fabian set up the optical lever again (the PR2 team had repossessed the breadboard we had been using but Akutsu-san supplied another one).
- Enzo and Mark tested the pico motors. The software is very unreliable, but we we able to confirm that the IM pitch pico works.
- The whole team wrapped items and shut down equipment ahead of the power outage.
Plan for coming weeks
For more detail, see KAGRA/Subgroups/VIS/TypeB/ToDo.
Week of 6/12:
- Cabling:
- Debug/fix PI vertical LVDTs #0 and #2.
- Calibrate PI vertical LVDT.
- Debug/fix geophone #1.
- Set yoke on PI vertical LVDT (if necessary).
- Cable and test PI yaw stepper.
- Cable and test PI vertical stepper.
- Cable and test PI horizontal steppers.
- Cable and test PI horizontal LVDTs.
- Calibrate PI horizontal LVDTs.
- Prepare LBB.
- Attach LBB outriggers and rod receptacles.
- Prepare LBB Cu ring.
- Remove from tank, fix incompletely threaded holes, reinstall in tank.
- Lay down spacers to protect magnets (in next step).
- Prepare LBB magnet ring.
- Disassemble.
- Pass pieces into tank.
- Reassemble on top of Cu ring.
- Install LBB damper.
- Bind LBB damper rings together with slings.
- Remove vacuum tank lid and ring.
- Crane rings up to install height, hook LBB magnet ring and support LBB Cu ring by TBD method.
- Crane suspension into tank.
- Hook LBB Cu ring.
- Hook LBB.
- Crane vacuum tank lid+ring black on.
- Remove vacuum tank lid (only).
- Remove port covers where feedthroughs will go, move feedthroughs from assembly frame and install on vacuum tank ring.
- Reconnect in-air cables.