Differences between revisions 156 and 200 (spanning 44 versions)
Revision 156 as of 2017-06-09 13:44:22
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Editor: MarkBarton
Comment:
Revision 200 as of 2017-10-13 14:57:07
Size: 2919
Editor: MarkBarton
Comment:
Deletions are marked like this. Additions are marked like this.
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At Kamioka (Mark, Fabian, Enzo, Hirata-san):
 * Hirata-san and Mark reversed the support ring for the LBB damper to match the reversed suspension.
 * Hirata-san did a trial assembly of the magnet ring for the LLB damper and placed magnets on it with the template.
 * Hirata-san and Mark put the base pieces for the Cu ring in the chamber. However it turns out that the holes for attaching the joint pieces are incompletely threaded and we will have to run a tap through them.
 * We tested the geophones. At first one didn't work at all. This turned out to be a broken wire in one of the in-vacuum adapter cables. For the test we replaced the adapter with an old-style one (and removed the matching descrambler). A second geophone mostly works but saturates at a suspiciously low number of counts at the ADC (2000 instead of 20000).
 * We tested the PI horizontal LVDTs. The #1 (H2) one works but cable swaps showed that #0 and #2 have issues both at the tank end and at the card.
 * We decided on a final location for the stepper and pico drivers on the second floor. We moved the cables for the stepper drivers (using the outside cable trays) and laid new LAN and AC cables for the picos.
 * We recounted the used and spare cables now that the in-vacuum cabling appears to be final.
At Kamioka (Mark, Ohishi-san, Fabian, Enzo, Hirata-san, Kozu-kun):
 * We couldn't account for a bubble level, so we removed a service port cover, searched again on top of the BF and found it.
 * We put the table KOACH filters on the table. Ohishi-san then removed the FC in two stages (AR side on Tue, HR side on Fri).
 * Ohishi-san measured the height of the SS and optic relative to the tank and found the optic was 3 mm low but the SS was 2 mm high. According to the GAS LVDTs, the suspension had not sagged but was 1.7 mm high.
 * Therefore we raised the suspension by 9 quarter-turns of the tank jacks (4.5 mm) so that the optic would be in the right position after (future) downward adjustment of the GAS filters.
 * We put the GAS LVDT calibration data as offsets and gains in the LVDTINF filters so the output would be height in µm relative to nominal.
 * We calibrated the IP LVDTs. We had worked around a mechanical interference due to the poor design of the old LVDTs by setting them to be 4 mm off-center with the IP locked centrally, but we discovered this was overkill and we have lost some linear range on the LVDT sensor in the opposite direction. If we have time we may move the LVDT bases 1-2 mm to a compromise position.
 * We worked with Simon to get the OL aligned and to learn the adjustment procedure.
 * Mark updated Sekiguchi-san's SUMCON to allow for comments to be entered next to all values (75% finished).
 * Kozu-kun worked on deriving the diagonalization matrices for the IP FRs.
 
At Mitaka (Hirata-san):
 * Hirata-san met with manufacturers and requested quotes.
 * Hirata-san made many assembly drawings for sections of the SR.
 * Hirata-san worked on compiling the SR inventory.
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==== Plan for coming weeks ====
For more detail, see [[KAGRA/Subgroups/VIS/TypeB/ToDo]].
==== Plan for week of 10/16 ====
Kamioka: all but Mark
 * Remove sticker residue and permanent marker writing on PI.
 * Fix broken and unreliable connections on IP LVDTs.
 * Wipe any rust from around IP LVDTs.
 * (If Enzo thinks it necessary and there's time) adjust IP LVDT mechanical offsets to maximize usable range and recalibrate.
 * Add IP LVDT gains and offsets to IP_LVDTINF filter blocks.
 * Calibrate IP LVDT actuation against IP LVDT sensing.
 * Install damping filters for IP LVDTs.
 * Adjust gains and debug damping for IM OSEMs and GAS LVDTs.
 * Modify IP LVDT damping filters to include set point.
 * Install and debug IP LVDT and geophone diagonalization matrices.
 * (Time permitting) Try adding mass to IP.
 * Work with alignment team.
 * Work with Mirapro on SR LBB and tank installation (Hirata-san, from Wed)
 * Work with Miyo-kun to get user interface for stepper motors.
 * Calibrate IP FR actuation against IP LVDT sensing.
 * SR procurement.
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Week of 6/12:
 * Cabling:
  * Debug/fix PI vertical LVDTs #0 and #2.
  * Calibrate PI vertical LVDT.
  * Debug/fix geophone #1.
  * Set yoke on PI vertical LVDT (if necessary).
  * Cable and test PI yaw stepper.
  * Cable and test PI vertical stepper.
  * Cable and test PI horizontal steppers.
  * Cable and test PI horizontal LVDTs.
  * Calibrate PI horizontal LVDTs.
 * Prepare LBB.
  * Attach LBB outriggers and rod receptacles.
 * Prepare LBB Cu ring.
  * Remove from tank, fix incompletely threaded holes, reinstall in tank.
  * Lay down spacers to protect magnets (in next step).
 * Prepare LBB magnet ring.
  * Disassemble.
  * Pass pieces into tank.
  * Reassemble on top of Cu ring.
 * Install LBB damper.
  * Bind LBB damper rings together with slings.
  * Remove vacuum tank lid and ring.
  * Crane rings up to install height, hook LBB magnet ring and support LBB Cu ring by TBD method.
 * Crane suspension into tank.
 * Hook LBB Cu ring.
 * Hook LBB.
 * Crane vacuum tank lid+ring black on.
 * Remove vacuum tank lid (only).
 * Remove port covers where feedthroughs will go, move feedthroughs from assembly frame and install on vacuum tank ring.
 * Reconnect in-air cables.
==== Vacation Info ====
Mark: 10/16-24

Scraps of text for incorporation in the VIS Meeting Minutes

KAGRA/Subgroups/VIS/MeetingNAOJ

Type B (Mark)

Past week report

At Kamioka (Mark, Ohishi-san, Fabian, Enzo, Hirata-san, Kozu-kun):

  • We couldn't account for a bubble level, so we removed a service port cover, searched again on top of the BF and found it.
  • We put the table KOACH filters on the table. Ohishi-san then removed the FC in two stages (AR side on Tue, HR side on Fri).
  • Ohishi-san measured the height of the SS and optic relative to the tank and found the optic was 3 mm low but the SS was 2 mm high. According to the GAS LVDTs, the suspension had not sagged but was 1.7 mm high.
  • Therefore we raised the suspension by 9 quarter-turns of the tank jacks (4.5 mm) so that the optic would be in the right position after (future) downward adjustment of the GAS filters.
  • We put the GAS LVDT calibration data as offsets and gains in the LVDTINF filters so the output would be height in µm relative to nominal.
  • We calibrated the IP LVDTs. We had worked around a mechanical interference due to the poor design of the old LVDTs by setting them to be 4 mm off-center with the IP locked centrally, but we discovered this was overkill and we have lost some linear range on the LVDT sensor in the opposite direction. If we have time we may move the LVDT bases 1-2 mm to a compromise position.
  • We worked with Simon to get the OL aligned and to learn the adjustment procedure.
  • Mark updated Sekiguchi-san's SUMCON to allow for comments to be entered next to all values (75% finished).
  • Kozu-kun worked on deriving the diagonalization matrices for the IP FRs.

At Mitaka (Hirata-san):

  • Hirata-san met with manufacturers and requested quotes.
  • Hirata-san made many assembly drawings for sections of the SR.
  • Hirata-san worked on compiling the SR inventory.

Plan for week of 10/16

Kamioka: all but Mark

  • Remove sticker residue and permanent marker writing on PI.
  • Fix broken and unreliable connections on IP LVDTs.
  • Wipe any rust from around IP LVDTs.
  • (If Enzo thinks it necessary and there's time) adjust IP LVDT mechanical offsets to maximize usable range and recalibrate.
  • Add IP LVDT gains and offsets to IP_LVDTINF filter blocks.
  • Calibrate IP LVDT actuation against IP LVDT sensing.
  • Install damping filters for IP LVDTs.
  • Adjust gains and debug damping for IM OSEMs and GAS LVDTs.
  • Modify IP LVDT damping filters to include set point.
  • Install and debug IP LVDT and geophone diagonalization matrices.
  • (Time permitting) Try adding mass to IP.
  • Work with alignment team.
  • Work with Mirapro on SR LBB and tank installation (Hirata-san, from Wed)
  • Work with Miyo-kun to get user interface for stepper motors.
  • Calibrate IP FR actuation against IP LVDT sensing.
  • SR procurement.

Vacation Info

Mark: 10/16-24

KAGRA/Subgroups/VIS/TypeB/Minutes (last edited 2022-10-28 10:02:46 by fabian.arellano)