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Revision 158 as of 2017-06-16 13:36:45
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Revision 217 as of 2018-01-19 13:48:30
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==== Past week report ====
At Kamioka (Mark, Fabian, Enzo, Hirata-san):
 * Hirata-san and Sekine-san moved the tank lid and service port ring to the pallet with the crane and covered the open tank with the spare clean bag.
 * Hirata-san and Mark got the LBB damper rings assembled and installed. A joint part for the Cu ring needed to have holes enlarged because the hole pattern did not quite match that on the half-ring. The magnet ring is hanging in the chamber and the Cu ring is attached below it with clamps, ready to receive the rods that will hang down from the PI.
 * Hirata-san recounted all the unused cables.
 * Hirata-san installed the outrigger parts on the LBB, which will receive the rods coming down from the damper ring.
 * Enzo and Mark tested all the stepper motors.
 * Enzo and Mark debugged the PI horizontal LVDTs. One LVDT had a flaky connection and one card in the LVDT driver had three dead channels. Enzo created a fully working driver using parts from another driver that also had a faulty card.
 * Fabian adjusted the ballast mass on the SF to get good pitch/roll/vertical adjustment and attached it with screws.
 * Fabian set up the optical lever again (the PR2 team had repossessed the breadboard we had been using but Akutsu-san supplied another one).
 * Enzo and Mark tested the pico motors. The software is very unreliable, but we we able to confirm that the IM pitch pico works.
 * The whole team wrapped items and shut down equipment ahead of the power outage.
==== Plan for coming weeks ====
For more detail, see [[KAGRA/Subgroups/VIS/TypeB/ToDo]].
==== Report for week of 1/15 ====
 * We set up the QPD for the OL, initialized the OL and TM sections of the RTM, and did TFs from the TM OSEMs to the OL.
 * Initially we had no coherence, but we debugged issues with the watchdog, LPCD, and DAC board and then got good TFs.
 * We lifted the IM/RM/SR with the load gauge adapter and checked the weight, which was close to the mass budget.
 * We installed the section of the AF above the IM, and the BF cross bars and jacks, and craned in the BF.
 * We installed the BF-IRM rods, IRM, BF-IM rod, flying saucer and the cable clamps on the bottom of the BF.
 * We hooked the IM section, but found it was heavy by several hundred grams. We also noticed the BF keystone had a noticeable tilt of about 1.2 mm (high on the +X side).
 * We removed 738 g of trim mass and found that load rose and sat about 2 mm high. So the discrepancy is of order 500-600 g.
 * Shoda-san, Enzo and Kozu-kun made and characterized a batch of OSEMs.
 * Hirata-san finished drawings for the improved BS PI yaw/vertical adjustment, placed orders for damping ring receptacles and other items, and prepared the second SR BF in case we needed to swap it in.
 
==== Plan for week of 1/22 ====
 * Fix or swap BF.
 * Route selected cables to flange.
 * Test IM picos and BF yaw pico.
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Week of 6/12:
 * Cabling:
  * Debug/fix PI vertical LVDTs #0 and #2.
  * Calibrate PI vertical LVDT.
  * Debug/fix geophone #1.
  * Set yoke on PI vertical LVDT (if necessary).
  * Cable and test PI yaw stepper.
  * Cable and test PI vertical stepper.
  * Cable and test PI horizontal steppers.
  * Cable and test PI horizontal LVDTs.
  * Calibrate PI horizontal LVDTs.
 * Prepare LBB.
  * Attach LBB outriggers and rod receptacles.
 * Prepare LBB Cu ring.
  * Remove from tank, fix incompletely threaded holes, reinstall in tank.
  * Lay down spacers to protect magnets (in next step).
 * Prepare LBB magnet ring.
  * Disassemble.
  * Pass pieces into tank.
  * Reassemble on top of Cu ring.
 * Install LBB damper.
  * Bind LBB damper rings together with slings.
  * Remove vacuum tank lid and ring.
  * Crane rings up to install height, hook LBB magnet ring and support LBB Cu ring by TBD method.
 * Crane suspension into tank.
 * Hook LBB Cu ring.
 * Hook LBB.
 * Crane vacuum tank lid+ring black on.
 * Remove vacuum tank lid (only).
 * Remove port covers where feedthroughs will go, move feedthroughs from assembly frame and install on vacuum tank ring.
 * Reconnect in-air cables.
==== Plan for week of 1/29 ====
 * Enzo at Mitaka 1/29 and most of 1/30, then vacation.
 * Kozu-kun away.
 * All others at Kamioka.
 * Build IRM around IM.
 * Cable/test/adjust IM OSEMs.
 * Time permitting, do TFs from IM OSEMs to themselves and to optical sensor.

==== Vacation Info ====
 * Enzo 1/30-2/19 (at Mitaka 1/29, part of 1/30)
 * Kozu-kun 1/29-2/2

Scraps of text for incorporation in the VIS Meeting Minutes

KAGRA/Subgroups/VIS/MeetingNAOJ

Type B (Mark)

Report for week of 1/15

  • We set up the QPD for the OL, initialized the OL and TM sections of the RTM, and did TFs from the TM OSEMs to the OL.
  • Initially we had no coherence, but we debugged issues with the watchdog, LPCD, and DAC board and then got good TFs.
  • We lifted the IM/RM/SR with the load gauge adapter and checked the weight, which was close to the mass budget.
  • We installed the section of the AF above the IM, and the BF cross bars and jacks, and craned in the BF.
  • We installed the BF-IRM rods, IRM, BF-IM rod, flying saucer and the cable clamps on the bottom of the BF.
  • We hooked the IM section, but found it was heavy by several hundred grams. We also noticed the BF keystone had a noticeable tilt of about 1.2 mm (high on the +X side).
  • We removed 738 g of trim mass and found that load rose and sat about 2 mm high. So the discrepancy is of order 500-600 g.
  • Shoda-san, Enzo and Kozu-kun made and characterized a batch of OSEMs.
  • Hirata-san finished drawings for the improved BS PI yaw/vertical adjustment, placed orders for damping ring receptacles and other items, and prepared the second SR BF in case we needed to swap it in.

Plan for week of 1/22

  • Fix or swap BF.
  • Route selected cables to flange.
  • Test IM picos and BF yaw pico.

Plan for week of 1/29

  • Enzo at Mitaka 1/29 and most of 1/30, then vacation.
  • Kozu-kun away.
  • All others at Kamioka.
  • Build IRM around IM.
  • Cable/test/adjust IM OSEMs.
  • Time permitting, do TFs from IM OSEMs to themselves and to optical sensor.

Vacation Info

  • Enzo 1/30-2/19 (at Mitaka 1/29, part of 1/30)
  • Kozu-kun 1/29-2/2

KAGRA/Subgroups/VIS/TypeB/Minutes (last edited 2022-10-28 10:02:46 by fabian.arellano)