Differences between revisions 16 and 140 (spanning 124 versions)
Revision 16 as of 2016-05-19 14:58:05
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Editor: MarkBarton
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Revision 140 as of 2017-04-27 19:31:10
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Editor: MarkBarton
Comment:
Deletions are marked like this. Additions are marked like this.
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 * Type B Past Week Summary
  * Flags and metal prisms ordered; expected 5/31.
  * New assembly drawing [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=5179| D1605179]] focussing on items not part of main chain (and associated screws):
   * Crane adapter
   * Lower breadboard blade module (with cable clamps)
   * IM-RM safety bar ([[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=5127| D1605127]] from last week now obsolete)
  * 3D assembly changed to have geophones instead of accelerometers (but SRx will probably be per original design - need to revisit circuit diagram)
  * Concept for load gauge adapter decided (reuse crane adapter plate and jacks from below PI; add Misumi crossbars, cleanroom-compatible chain hoist: [[attachment: Crane Frame.pdf]])
  * Concept for second floor of clean booth decided (remove all floor panels; add bridge panels at right angles: [[attachment:BS Cleanbooth.pdf]])
  * Modified drawings for main assembly frame and drawings for most small parts (jack adapters etc) received from Mirapro.
  * Wire sizes decided: 300 µm piano wire and 500 µm tungsten (will revisit this later).
  * Lots of work on [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=4817| E1604817]] (Fabian; [[https://onedrive.live.com/redir?resid=D5CCFA70A378E0D0!191&authkey=!AMe0pdcd9GDm1H0&ithint=folder%2cwebloc|Draft on OneDrive]]) and [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=4235| E1504235]] (Mark; [[https://onedrive.live.com/redir?resid=D5CCFA70A378E0D0!195&authkey=!AM_usynuo9QI57g&ithint=folder%2cwebloc|Draft on OneDrive]])
=== Type B (Mark) ===
==== Past week report ====
At Kamioka (Mark, Fabian, Enzo, Perry, Hirata-san):
Line 18: Line 9:
 * Type B Past Week Summary
  * Fabian did inventory of parts/fasteners for dummy BS, RM, IM and IRM - almost all at Mitaka. A handful (picos, pico drivers) will be brought back from Kamioka.
  * Fabian continued work on Mathematica and Matlab models of the BS and control system. He now gets much better agreement after correcting discrepancies between the parameter sets.
  * Hirata-san worked on organizing:
   * Work platforms
   * Load gauge adapter and associated parts
   * Possible fall-back plans for the rods connecting the security structure to the PI.
 * We craned in the PI.
 * We assembled the thrust bearing holder that receives the PI-SF rod. (The recess for the bearing was very slightly too small and had a burr near a retaining screw hole that prevented the bearing from seating properly, and so it required filing and re-cleaning.)
 * We hooked the SF and lowered the jacks under the SF to suspend the SF/... section.
 * The top filter rose when unlocked, and required about 1.8 kg to send it back down. Therefore we may be OK - the top filter seems to have about 8 kg more capacity than as measured by G&M. The hex cable clamp (≈0.25 kg) and the cables between the PI and SF still have to be added, but we can get an extra 3 kg by removing one of the three Cu damper segments (and rearranging the other two).
 * Hirata-san built and installed three LBB blade units.
 * Enzo kept debugging the SF LVDT. We repaired several broken wires, but it's still not behaving correctly. We suspect the ordering of the three coils (input output and excitation) may not be right. If so, we should be able to fix it with an adapter cable without removing the SF cap.

==== Plan for coming weeks ====
For more detail, see [[KAGRA/Subgroups/VIS/TypeB/ToDo]].

Week of 5/1:
 * No activity (Golden Week).

Week of 5/8:
 * Commence work Tuesday 5/9.
 * Remove PI temporarily.
 * Continue debugging SF LVDT (removing cap if necessary).
 * Investigate possible mis-alignment between the tips of the LBB blades and the holes for the rods going down to the damper ring.
 * Add magnets to upper SF damper ring.
 * Reinstall PI, this time with rods and damper ring.
 * Reinstall PI-SF rod, this time with hex cable clamp.
 * Install PI yaw stepper.
 * Wire up PI yaw stepper and vertical fishing-rod steppers.
 * Route cables from SF to PI (may involve removing part of Cu damper).

Week of 5/15:
 * Enzo from Tuesday 5/16 (driving test), rest of team from Monday.
 * Prepare for PR2 bellows removal on 5/15 (move table with tools).
 * Wire up PI horizontal LVDTs and steppers.
 * Install geophones.
 * Unlock IP, re-level PI to center PI, add arc weights as required.
 

Scraps of text for incorporation in the VIS Meeting Minutes

KAGRA/Subgroups/VIS/MeetingNAOJ

Type B (Mark)

Past week report

At Kamioka (Mark, Fabian, Enzo, Perry, Hirata-san):

  • We craned in the PI.
  • We assembled the thrust bearing holder that receives the PI-SF rod. (The recess for the bearing was very slightly too small and had a burr near a retaining screw hole that prevented the bearing from seating properly, and so it required filing and re-cleaning.)
  • We hooked the SF and lowered the jacks under the SF to suspend the SF/... section.
  • The top filter rose when unlocked, and required about 1.8 kg to send it back down. Therefore we may be OK - the top filter seems to have about 8 kg more capacity than as measured by G&M. The hex cable clamp (≈0.25 kg) and the cables between the PI and SF still have to be added, but we can get an extra 3 kg by removing one of the three Cu damper segments (and rearranging the other two).

  • Hirata-san built and installed three LBB blade units.
  • Enzo kept debugging the SF LVDT. We repaired several broken wires, but it's still not behaving correctly. We suspect the ordering of the three coils (input output and excitation) may not be right. If so, we should be able to fix it with an adapter cable without removing the SF cap.

Plan for coming weeks

For more detail, see KAGRA/Subgroups/VIS/TypeB/ToDo.

Week of 5/1:

  • No activity (Golden Week).

Week of 5/8:

  • Commence work Tuesday 5/9.
  • Remove PI temporarily.
  • Continue debugging SF LVDT (removing cap if necessary).
  • Investigate possible mis-alignment between the tips of the LBB blades and the holes for the rods going down to the damper ring.
  • Add magnets to upper SF damper ring.
  • Reinstall PI, this time with rods and damper ring.
  • Reinstall PI-SF rod, this time with hex cable clamp.
  • Install PI yaw stepper.
  • Wire up PI yaw stepper and vertical fishing-rod steppers.
  • Route cables from SF to PI (may involve removing part of Cu damper).

Week of 5/15:

  • Enzo from Tuesday 5/16 (driving test), rest of team from Monday.
  • Prepare for PR2 bellows removal on 5/15 (move table with tools).
  • Wire up PI horizontal LVDTs and steppers.
  • Install geophones.
  • Unlock IP, re-level PI to center PI, add arc weights as required.

KAGRA/Subgroups/VIS/TypeB/Minutes (last edited 2022-10-28 10:02:46 by fabian.arellano)