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* Type B Past Week Summary * Flags and metal prisms ordered; expected 5/31. * New assembly drawing [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=5179| D1605179]] focussing on items not part of main chain (and associated screws): * Crane adapter * Lower breadboard blade module (with cable clamps) * IM-RM safety bar ([[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=5127| D1605127]] from last week now obsolete) * 3D assembly changed to have geophones instead of accelerometers (but SRx will probably be per original design - need to revisit circuit diagram) * Concept for load gauge adapter decided (reuse crane adapter plate and jacks from below PI; add Misumi crossbars, cleanroom-compatible chain hoist: [[attachment: Crane Frame.pdf]]) * Concept for second floor of clean booth decided (remove all floor panels; add bridge panels at right angles: [[attachment:BS Cleanbooth.pdf]]) * Modified drawings for main assembly frame and drawings for most small parts (jack adapters etc) received from Mirapro. * Wire sizes decided: 300 µm piano wire and 500 µm tungsten (will revisit this later). * Lots of work on [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=4817| E1604817]] (Fabian; [[https://onedrive.live.com/redir?resid=D5CCFA70A378E0D0!191&authkey=!AMe0pdcd9GDm1H0&ithint=folder%2cwebloc|Draft on OneDrive]]) and [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=4235| E1504235]] (Mark; [[https://onedrive.live.com/redir?resid=D5CCFA70A378E0D0!195&authkey=!AM_usynuo9QI57g&ithint=folder%2cwebloc|Draft on OneDrive]]) * Type B Past Week Summary * Fabian did inventory of parts/fasteners for dummy BS, RM, IM and IRM - almost all at Mitaka. A handful (picos, pico drivers) will be brought back from Kamioka. * Fabian continued work on Mathematica and Matlab models of the BS and control system. He now gets much better agreement after correcting discrepancies between the parameter sets. * Hirata-san worked on organizing: * Work platforms * Load gauge adapter and associated parts * Possible fall-back plans for the rods connecting the security structure to the PI. |
* Mark, Fabian and Enzo continued BS Test Hang work: * We installed the BF fishing rod stepper motor adaptor cable. * We tried to install the BF LVDT cable but first we encountered trouble routing it, and then several wires broke at the D-Sub end. * We laid 6 in-air cables from the tank to the PR2 rank for BF and SF picos, steppers and LVDTs. * We lifted the BF/IRM/IM/RM/BS section to weigh it and check its balance. * It was 195.6 kg, which is 18 kg(!) less than the capacity of the SF. * There was a major imbalance in roll: with all four built-in trim masses moved up the +Y end, it still needed 270 g of extra trim mass to be level. * Unfortunately when we put the payload, the IM was slightly yawed and ended up on the horizontal EQ stop screws. This let the IM-BF maraging rod go slack, which disturbed the leveling of the IM (because every time it is picked up the maraging rod settles in a different place, giving a different suspension point). We may have to partly disassemble the IRM and rearrange the time mass on the the IM. * We shipped BS mirror box parts to Shoda-san and components for a new LVDT cable to Hirata-san. * We posed for pictures of the BS by a team from National Geographic. * Hirata-san * Did parts and fastener lists for the SR payload. * Did a 3D model with the SR suspension on the BS assembly frame (to help Mark make adjustments to the frame design). * Did 2D drawings of Fabian's concept for BS EQ stop parts. * Did a 3D model of a wire clamp with replaceable jaw parts (to avoid having to reuse parts with scars from pressure). * Did 2D drawings of a new wire clamps for on top of the BS and SR RMs. |
Scraps of text for incorporation in the VIS Meeting Minutes
KAGRA/Subgroups/VIS/MeetingNAOJ
- Mark, Fabian and Enzo continued BS Test Hang work:
- We installed the BF fishing rod stepper motor adaptor cable.
- We tried to install the BF LVDT cable but first we encountered trouble routing it, and then several wires broke at the D-Sub end.
- We laid 6 in-air cables from the tank to the PR2 rank for BF and SF picos, steppers and LVDTs.
- We lifted the BF/IRM/IM/RM/BS section to weigh it and check its balance.
- It was 195.6 kg, which is 18 kg(!) less than the capacity of the SF.
- There was a major imbalance in roll: with all four built-in trim masses moved up the +Y end, it still needed 270 g of extra trim mass to be level.
- Unfortunately when we put the payload, the IM was slightly yawed and ended up on the horizontal EQ stop screws. This let the IM-BF maraging rod go slack, which disturbed the leveling of the IM (because every time it is picked up the maraging rod settles in a different place, giving a different suspension point). We may have to partly disassemble the IRM and rearrange the time mass on the the IM.
- We shipped BS mirror box parts to Shoda-san and components for a new LVDT cable to Hirata-san.
- We posed for pictures of the BS by a team from National Geographic.
- Hirata-san
- Did parts and fastener lists for the SR payload.
- Did a 3D model with the SR suspension on the BS assembly frame (to help Mark make adjustments to the frame design).
- Did 2D drawings of Fabian's concept for BS EQ stop parts.
- Did a 3D model of a wire clamp with replaceable jaw parts (to avoid having to reuse parts with scars from pressure).
- Did 2D drawings of a new wire clamps for on top of the BS and SR RMs.