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 * Type B Past Week Summary
  * Fabian worked on IM and dummy BS assembly: [[https://photos.google.com/share/AF1QipMNVSExyP3TuyhK4s_VD-ARDlNoCPCf13ZDbHUlwOw14AKgj4XUe0vYg27dQ12icQ?key=SjJ0dXJ1bjN2OGVCN3d6RnoySEtFSjVJUmVwSlZR|photos1]], [[https://photos.google.com/share/AF1QipPQdoB5vYN1VcD32TkA4QSGldODvKRwiT5h-m122ahSpWmFyyrO5MX-9ajL1LeRIg?key=VFFuUVktcEtlMURQUldhZUlRcGFhbzNDeU5IN3NB|photos2]]
   * A hole in a picomotor holder was too small. ATC staff solved this isue quickly and Hirata-san cleaned the piece.
   * Some ballast discs for the dummy optic were dirty (seen by visual inspection). Hirata-san cleaned them.
   * Some arrows were cleaned from the mirrors for the dummy optic.
  * Hirata-san worked on checking Mirapro's assembly frame design - some minor issues with rail system found.
  * Hirata-san measured another filter.
  * Hirata-san washed a large batch of parts.
  * All parts for gluing of dummy BS are in hand. We arranged with Tatsumi-san to glue magnets at Mitaka on 6/6, glue flags at Kashiwa on 6/8, and inspect bonds and bring dummy BS back to Mitaka 6/13.
  * Mark worked on solutions to allow a [[http://gwwiki.icrr.u-tokyo.ac.jp/JGWwiki/KAGRA/Subgroups/VIS/TypeB/dummyBS|larger mirror on dummy BS]]. After discussions with Simon and Akutsu-san we decided to go with a stainless steel plate solution. The gluing can go ahead and we can attach the plates later.
  * Mark worked on list of items for purchase in FY2016.
  * Mark worked on finding connectors for vacuum-compatible geophone adapters.
  * Mark worked more on [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=4235|E1504235 BS Assembly Procedure]] ([[https://onedrive.live.com/redir?resid=D5CCFA70A378E0D0!195&authkey=!AM_usynuo9QI57g&ithint=folder,webloc|Draft on OneDrive]])
 * '''Discussions '''
  * Crane will not be available on 13-14 of June.
  * Review: '''fix the date (Mark) '''
  * Measurement of iKAGRA BS position will be done in the second week of June. Then it will be taken out of the chamber after that (Ohishi)
 * IM, RM, IRM, dummy BS assembly
  * Fabian assembled the dummy BS and started on the IM.
  * Still need to find SDC-treated hook for maraging wire in IM. Still not found. Spare hook is being SDC-treated. Can be added later.
  * Will start assembly 5/30
 * Wires
  * Fabian analysis RM wire thickness versus mode frequency: [[https://onedrive.live.com/redir?resid=1447B05D5B571A84!442&authkey=!AKrjBW2W8vMKyAY&ithint=file,pdf|link]], [[https://onedrive.live.com/redir?resid=1447B05D5B571A84!421&authkey=!ALZY-tFtMCYI9Pw&ithint=file,pdf|another link]],[[https://pfalig.bn1301.livefilestore.com/y3mT7oHnuBfD9_7Ata6H90opTVY5IIIm78MQ8Rl-lChfSUtGhGiEP-mlB1rQuzliimi-pmL1JfYTKCUY_Tgan0Bfa2jq5EeSXWiCracw_5ulsm2iuf6RHJcz0ot34DaeWqdUjFnU6fILnyau69WFkBmUcTwfGYBNwSrs27eyK-jc90/RM_wire.pdf?psid=1|yet another link]] (From last week: [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=5106|T1605106]] /[[https://onedrive.live.com/view.aspx?resid=1447B05D5B571A84!354&ithint=file,docx&app=Word&authkey=!AO5CHNP3xlO5RjY|draft]])
 * Can we make SR wire breakers bigger?
  * Fukushima-san has not yet started the work. He will start soon (as of 5/27).
 * Flags, Metal Prisms, Sapphire prisms RECEIVED
 * Mirror box and Flag/Prism gluing
  * All parts in hand.
  * Magnet gluing and check of parts at Mitaka, Monday 6/6.
  * Gluing at Kashiwa, Wednesday 6/8.
  * Inspection of bonds and return to Mitaka, 6/13.
 * An extra structure attached to the EQ stop to prevent tipping over of the BS - no action since last week.
 * Not enough crane height problem (Hirata, Saito) - no action since last week
 * Ballast masses for payload
  * Initial batch received - ordered extra smaller ones to allow for adjustments.
 * Lower breadboard stuff
  * Assembly procedure
   * '''Need to be incorporated into the procedure document. Discuss with Takahashi (Mark)'''
  * Breadboard springs (in manufacture, expected end of July)
  * Nail-head parts: quote from Mirapro received, not urgent, will be combined with assembly frame order.
 * BS Assembly Frame Design (Mark, Hirata)
  * Hirata-san found issues with rail system part - organizing fix.
 * Clean bag
  * Ordered - expected 6/8.
 * 2D and 3D CAD
  * [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=5035|E1605035 VIS Document and Drawing Tree (BS)]]
 * Electronics
  * [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=3600|JGW-D1503600 - BS Suspension Cabling]]
  * [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=5111|E1605111 BS Suspension Electronic Items List]]
  * [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=3901|D1503901 In-Vacuum Cable Detail]]
  * Item list and timetable was given to Miyakawa-san - some corrections received and added to schematic but not yet posted.
  * Status on AEL boxes OK according to Miyakawa-san.
  * Signal generator and cable to be used for BS test. May order NIKHEF cards later if concern about AC-driven units in racks.
  * Need to get new longer versions of some previously ordered BF-PI and SF-PI cables (Takahashi).
  * Need to check previously ordered TM-BF and IM-BF OSEM cables have been flipped (Takahashi).
  * Decided to hand-make cables for geophones because previously ordered cables have no conductor on pin 5.
  * Stepper drive box (requested by Sekiguchi-san [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=3385|T1503385]]) is being designed, should be ready in time.
  * Mark looking for connectors for geophone adapters.
 * Procedure documents
  * Mark worked on BS Assembly Procedure [[https://onedrive.live.com/redir?resid=D5CCFA70A378E0D0!195&authkey=!AM_usynuo9QI57g&ithint=folder,webloc|E1504235 draft]]
=== Type B (Mark) ===
==== Report for week of 12/17 ====
 * BS
  * Miyakawa-san worked on the BS real-time model and the gain/offset settings for the F0 LVDTINF block were lost, so we reentered them and did a new safe.snap file.
 * SRM
  * We unlocked the IP adjusted the level with the jacks to center it. As hoped, this also improved the alignment of the chain insecurity structure and fixed a touching issue.
  * Hirata-san installed and cabled the new F0 yaw stepper. We had allowed plenty of reserve mass, so there was no problem getting back to nominal height of the keystone. [''As of Thursday afternoon, it had not yet been tested - UPDATE?'']
  * We found that the Nikhef method Fabian had used to tune the F0 LVDT driver gave an artificially narrow working range, so he retuned it with Enzo's method and recalibrated the LVDT.
  * Fabian did a vertical position survey with all the GAS filters at nominal and found the height of the RM above the SS bottom plate was about 2.5 mm lower than in the CAD. This is about what we expected from a chain 7 mm longer than CAD and and F0 keystone set to 5 mm higher than CAD. In future we can survey to either the optic or the security structure as convenient, and we are in the range where we should easily be able to match the correct beam height with the jacks under the PI.
  * We got two OL viewports for SRM from Akutsu-san, and will install them sometime in January, whenever we have a free moment. Akutsu-san pre-torqued the inner ring of screws around the glass, so we only need to torque the outer bolts.
  * We took transfer functions for the IM. All of them look good except IM-T. We will inspect the payload next week in case anything is touching or rubbing.
  * Hirata-san opened the +X door of the vacuum chamber for visual inspection. We closed it back and covered with tape a small gap at the door.
 * SR3
  * We also got a camera viewport for SR3 from Akutsu-san and will install it sometime in January.
  * Hirata-san installed and cabled the new F0 yaw stepper.
 * SR2
  * Enzo calibrated the SR2 OL. He noted that with the standard f=2500 mm collimator, the angular range was only about 100 µrad in pitch and 150 µrad in yaw, which is rather less than Enomoto-kun's preferred range of more like 400 µrad, so we borrowed f=1100 mm and f=3500 mm collimators to characterize. [''Enzo was going to do f=1100 mm and maybe f=3500 mm on Friday morning 12/21 - UPDATE?'']
  * Hirata-san installed and cabled the new F0 yaw stepper. We did not have enough reserve mass for SR2, so to save 300 g we had Mesco make a new, lighter top plate, and Hirata-san ultrasonically cleaned it. We were then able to get the desired F0 keystone height with about 200 g to spare.
  * The RM was touching the security structure due to a large yaw displacement. We were able to move it free by adjusting the cylinder with the spring and leaving the stepper motor in its nominal position. The f=1100 mm collimator was installed and the QPD was calibrated.
 * Etc
  * Enzo did a historical survey of the temperature as the various suspensions were being built and concluded that ideal operating temperature would be 25°C in the BS/SR2 area and 24°C for SR3/SRM.
  * Mark wrote a bash script to log all the GAS filter heights and LVDT actuation offsets, and an Excel spreadsheet to analyze the data to get an overview of the heights of the suspensions and the amount of height adjustment being used. He also reviewed old TF data to get near-DC values for the effect of GAS actuation on GAS height. This uncovered a few issues with calibration settings (such as for BS F0) having been lost because they hadn't been recorded in a safe.snap file, which we fixed.

==== To-Do Lists, Schedule ====
 * [[KAGRA/Subgroups/VIS/TypeB/ToDoBS]]
 * [[KAGRA/Subgroups/VIS/TypeB/ToDoSR]]
 * [[https://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=7779|JGW-L1807779 Type B Schedule (SR)]]

==== Plan for week of 12/17 ====
 * Final alignment of SRM payload, plus BF and SF GAS.
 * (Time permitting) unlocking/centering/tuning of IP.
 * Installation of Enomoto-kun's beam target on SRM (if available).
 * Installation/testing of F0 steppers on SR2, SR3, SRM, and (hopefully) final vertical height adjustment.
 * Installation of viewports on SRM.

==== Plan for week of 12/24 ====
 * Mark and Hirata-san on holidays, Enzo at Mitaka, Fabian.

==== Plan for week of 1/7 ====
 * Make sure BS is floating, recenter OL to capture current yaw position.
 * Vent BS.
 * Inspect BS F0 blades for cracks.
 * Install new BS F0 FR, and (if necessary) auxiliary CuBe spring.
 * Confirm geometry of LVDTs, geophones, FRs etc and update T1707205 if necessary.
 * Replace geophone preamps and cables (to fix noise, offset, pinout flip issues).
 * Add more mass to IP to get lower frequency.
 * Adjust all GAS filters to near mid-range (using keystone mass for F0 as much as possible, and FR+LVDT for SF and BF).

==== Vacation/Etc Info ====
 * Mark: 12/24 - 1/4.
 * Hirata-san: 12/24 - 1/4.
 * Fabian: 12/31 - 1/4
 * Enzo: 12/31 - 1/4.
 * Mark and Enzo: KAGRA International Workshop in Perugia, 2/14-16.
 * Terrence: back at Kamioka from 1/7.

Scraps of text for incorporation in the VIS Meeting Minutes

KAGRA/Subgroups/VIS/MeetingNAOJ

Type B (Mark)

Report for week of 12/17

  • BS
    • Miyakawa-san worked on the BS real-time model and the gain/offset settings for the F0 LVDTINF block were lost, so we reentered them and did a new safe.snap file.
  • SRM
    • We unlocked the IP adjusted the level with the jacks to center it. As hoped, this also improved the alignment of the chain insecurity structure and fixed a touching issue.
    • Hirata-san installed and cabled the new F0 yaw stepper. We had allowed plenty of reserve mass, so there was no problem getting back to nominal height of the keystone. [As of Thursday afternoon, it had not yet been tested - UPDATE?]

    • We found that the Nikhef method Fabian had used to tune the F0 LVDT driver gave an artificially narrow working range, so he retuned it with Enzo's method and recalibrated the LVDT.
    • Fabian did a vertical position survey with all the GAS filters at nominal and found the height of the RM above the SS bottom plate was about 2.5 mm lower than in the CAD. This is about what we expected from a chain 7 mm longer than CAD and and F0 keystone set to 5 mm higher than CAD. In future we can survey to either the optic or the security structure as convenient, and we are in the range where we should easily be able to match the correct beam height with the jacks under the PI.
    • We got two OL viewports for SRM from Akutsu-san, and will install them sometime in January, whenever we have a free moment. Akutsu-san pre-torqued the inner ring of screws around the glass, so we only need to torque the outer bolts.
    • We took transfer functions for the IM. All of them look good except IM-T. We will inspect the payload next week in case anything is touching or rubbing.
    • Hirata-san opened the +X door of the vacuum chamber for visual inspection. We closed it back and covered with tape a small gap at the door.
  • SR3
    • We also got a camera viewport for SR3 from Akutsu-san and will install it sometime in January.
    • Hirata-san installed and cabled the new F0 yaw stepper.
  • SR2
    • Enzo calibrated the SR2 OL. He noted that with the standard f=2500 mm collimator, the angular range was only about 100 µrad in pitch and 150 µrad in yaw, which is rather less than Enomoto-kun's preferred range of more like 400 µrad, so we borrowed f=1100 mm and f=3500 mm collimators to characterize. [Enzo was going to do f=1100 mm and maybe f=3500 mm on Friday morning 12/21 - UPDATE?]

    • Hirata-san installed and cabled the new F0 yaw stepper. We did not have enough reserve mass for SR2, so to save 300 g we had Mesco make a new, lighter top plate, and Hirata-san ultrasonically cleaned it. We were then able to get the desired F0 keystone height with about 200 g to spare.
    • The RM was touching the security structure due to a large yaw displacement. We were able to move it free by adjusting the cylinder with the spring and leaving the stepper motor in its nominal position. The f=1100 mm collimator was installed and the QPD was calibrated.
  • Etc
    • Enzo did a historical survey of the temperature as the various suspensions were being built and concluded that ideal operating temperature would be 25°C in the BS/SR2 area and 24°C for SR3/SRM.
    • Mark wrote a bash script to log all the GAS filter heights and LVDT actuation offsets, and an Excel spreadsheet to analyze the data to get an overview of the heights of the suspensions and the amount of height adjustment being used. He also reviewed old TF data to get near-DC values for the effect of GAS actuation on GAS height. This uncovered a few issues with calibration settings (such as for BS F0) having been lost because they hadn't been recorded in a safe.snap file, which we fixed.

To-Do Lists, Schedule

Plan for week of 12/17

  • Final alignment of SRM payload, plus BF and SF GAS.
  • (Time permitting) unlocking/centering/tuning of IP.
  • Installation of Enomoto-kun's beam target on SRM (if available).
  • Installation/testing of F0 steppers on SR2, SR3, SRM, and (hopefully) final vertical height adjustment.
  • Installation of viewports on SRM.

Plan for week of 12/24

  • Mark and Hirata-san on holidays, Enzo at Mitaka, Fabian.

Plan for week of 1/7

  • Make sure BS is floating, recenter OL to capture current yaw position.
  • Vent BS.
  • Inspect BS F0 blades for cracks.
  • Install new BS F0 FR, and (if necessary) auxiliary CuBe spring.

  • Confirm geometry of LVDTs, geophones, FRs etc and update T1707205 if necessary.
  • Replace geophone preamps and cables (to fix noise, offset, pinout flip issues).
  • Add more mass to IP to get lower frequency.
  • Adjust all GAS filters to near mid-range (using keystone mass for F0 as much as possible, and FR+LVDT for SF and BF).

Vacation/Etc Info

  • Mark: 12/24 - 1/4.
  • Hirata-san: 12/24 - 1/4.
  • Fabian: 12/31 - 1/4
  • Enzo: 12/31 - 1/4.
  • Mark and Enzo: KAGRA International Workshop in Perugia, 2/14-16.
  • Terrence: back at Kamioka from 1/7.

KAGRA/Subgroups/VIS/TypeB/Minutes (last edited 2022-10-28 10:02:46 by fabian.arellano)