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 * Type B Past Week Summary
  * Mark and Fabian worked at Kamioka with Fujii-san:
   * We attempted to measure the tilt sensitivity of the accelerometers by adding shims under the legs but gave up when we discovered that picking up and putting down the accelerometer perturbs the zero point even without shims. We will probably need a special tilt stage to do this properly.
   * We took some frequency and Q measurements. The results were amplitude dependent. Joris thinks that this is due to not operating the accelerometers close enough to zero DC output.
   * We set up for a test of the geophone noise. One geophone is reading half the output of the others - one of the adapter cables is broken.
  * Hirata-san:
   * Received extra compensation masses and washed them.
   * Received PI guides, assembled them and shipped them to Kamioka.
   * Received backup set of pillar for security structure (with M10 instead of M12 holes at top).
   * Removed adhesive from base of BS flags in preparation for regluing.
   * Did assembly drawings for cable clamps and other add-on parts for BF and SF.
 * Type B ongoing issues
  * Wires
   * Need to decide RM wire thickness and order BS and RM wires. Lead time is a few days from Nilaco.
  * OSEMs
   * Akutsu-san is working to get wide-mouth OSEMs
  * Longer cables for BF->PI and SF->PI.
   * Connectors RECEIVED, cables being made.
  * Feedthrough Adapters
   * Connectors RECEIVED.
  * SR machining test ONGOING.
  * Installation stuff
   * "Ceiling" work in BS clean booth (removal of second floor section) scheduled for Fri 7/1.
   * Assembly frame construction scheduled for 7/4
  * Ballast masses for payload
   * Initial batch received - ordered extra smaller ones to allow for adjustments.
  * Lower breadboard stuff
   * Installation to be incorporated into the procedure document. Mark/Takahashi to discuss.
   * Breadboard springs (in manufacture, expected end of July)
   * Nail-head parts - ordered with assembly frame, will arrive next week.
  * Documents
   * BS Assembly Procedure [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=4235| E1504235]], [[https://onedrive.live.com/redir?resid=D5CCFA70A378E0D0!195&authkey=!AM_usynuo9QI57g&ithint=folder,webloc|E1504235 draft]]
=== Type B (Mark) ===
==== Past week report ====
At Kamioka (Mark, Fabian, Enzo, Perry, Hirata-san):

 * Filed crane adapter ring to make it fit better on the hook.
 * Debugged the BF and SF LVDTs (the signal generator had lost its settings in the rack shutdown).
 * Debugged the TM-H4 OSEM problem (a "Type 3 extension cable had gone bad).
 * Weighed eyebolts used to lie the SF.
 * Shipped the old pico driver and joystick back to Mitaka for Eleonora.
 * Borrowed a second pico driver ("PR3") and set it and "BS" up in the rack.
 * Practiced driving the BF cap picos with the new drivers.
 * (With help from Miyo-kun) got the pico MEDM screens running.
 * Replace the temporary "PR3" driver with a new one "BS_BF", and renamed "BS" to "BS_IM".
 * Checked all the DIO connections to the LPCD and connected up the HPCDs. With help from Kokeyama-san we can now see all the drivers from EPICS.
 * Worked on balancing the BF/IRM/IM... section. Sometime during this work, the IM sank and would not come back to its proper position even with the fishing rod. We put a scale under the RM and found that the imbalance was 488 g. Using the fishing rod we got this down to 235 g, but we found that the direction of the stepper was not consistently related to the direction selected on the driver screen - we had previously noted that "left" was "up, but driving "up" the imbalance would decrease to 235 g and then start increasing again, indicating the stepper had bounced off some obstacle. (There was no obvious sound when this happened, unlike at the low end.)
 * We decided to give up on tuning the height of the IM with the fishing rod and to proceed with the test hang by locking the BF keystone at the desired height.
 * Hirata-san installed the PI fishing rod and magic wand, and did more work on changing the PI LVDT connectors from female to male.
 * Enzo made many edits to the circuit diagram, adding the DIO for the HPCDs and correcting minor mistakes.

==== Plan for coming weeks ====
For more detail, see [[KAGRA/Subgroups/VIS/TypeB/ToDo]].

Week of 4/17:
 * Install temporary ballast mass in SF.
 * Lift SF/BF/... section and check total weight and SF balance.
 * Continue swap of PI LVDT connectors (female->male)
 * Start preparing LBB spring units.
Week of 4/24:
 * Crane in PI.
 * Connect SF/BF... section.
 * Temporarily remove PI and adjust SF ballast if necessary.
 

Scraps of text for incorporation in the VIS Meeting Minutes

KAGRA/Subgroups/VIS/MeetingNAOJ

Type B (Mark)

Past week report

At Kamioka (Mark, Fabian, Enzo, Perry, Hirata-san):

  • Filed crane adapter ring to make it fit better on the hook.
  • Debugged the BF and SF LVDTs (the signal generator had lost its settings in the rack shutdown).
  • Debugged the TM-H4 OSEM problem (a "Type 3 extension cable had gone bad).
  • Weighed eyebolts used to lie the SF.
  • Shipped the old pico driver and joystick back to Mitaka for Eleonora.
  • Borrowed a second pico driver ("PR3") and set it and "BS" up in the rack.
  • Practiced driving the BF cap picos with the new drivers.
  • (With help from Miyo-kun) got the pico MEDM screens running.
  • Replace the temporary "PR3" driver with a new one "BS_BF", and renamed "BS" to "BS_IM".
  • Checked all the DIO connections to the LPCD and connected up the HPCDs. With help from Kokeyama-san we can now see all the drivers from EPICS.
  • Worked on balancing the BF/IRM/IM... section. Sometime during this work, the IM sank and would not come back to its proper position even with the fishing rod. We put a scale under the RM and found that the imbalance was 488 g. Using the fishing rod we got this down to 235 g, but we found that the direction of the stepper was not consistently related to the direction selected on the driver screen - we had previously noted that "left" was "up, but driving "up" the imbalance would decrease to 235 g and then start increasing again, indicating the stepper had bounced off some obstacle. (There was no obvious sound when this happened, unlike at the low end.)
  • We decided to give up on tuning the height of the IM with the fishing rod and to proceed with the test hang by locking the BF keystone at the desired height.
  • Hirata-san installed the PI fishing rod and magic wand, and did more work on changing the PI LVDT connectors from female to male.
  • Enzo made many edits to the circuit diagram, adding the DIO for the HPCDs and correcting minor mistakes.

Plan for coming weeks

For more detail, see KAGRA/Subgroups/VIS/TypeB/ToDo.

Week of 4/17:

  • Install temporary ballast mass in SF.
  • Lift SF/BF/... section and check total weight and SF balance.
  • Continue swap of PI LVDT connectors (female->male)

  • Start preparing LBB spring units.

Week of 4/24:

  • Crane in PI.
  • Connect SF/BF... section.
  • Temporarily remove PI and adjust SF ballast if necessary.

KAGRA/Subgroups/VIS/TypeB/Minutes (last edited 2022-10-28 10:02:46 by fabian.arellano)