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 * Type B Past Week Summary
  * Mark and Fabian worked at Kamioka with Fujii-san:
   * We attempted to measure the tilt sensitivity of the accelerometers by adding shims under the legs but gave up when we discovered that picking up and putting down the accelerometer perturbs the zero point even without shims. We will probably need a special tilt stage to do this properly.
   * We took some frequency and Q measurements. The results were amplitude dependent. Joris thinks that this is due to not operating the accelerometers close enough to zero DC output.
   * We set up for a test of the geophone noise. One geophone is reading half the output of the others - one of the adapter cables is broken.
  * Hirata-san:
   * Received extra compensation masses and washed them.
   * Received PI guides, assembled them and shipped them to Kamioka.
   * Received backup set of pillar for security structure (with M10 instead of M12 holes at top).
   * Removed adhesive from base of BS flags in preparation for regluing.
   * Did assembly drawings for cable clamps and other add-on parts for BF and SF.
 * Type B ongoing issues
  * Wires
   * Need to decide RM wire thickness and order BS and RM wires. Lead time is a few days from Nilaco.
  * OSEMs
   * Akutsu-san is working to get wide-mouth OSEMs
  * Longer cables for BF->PI and SF->PI.
   * Connectors RECEIVED, cables being made.
  * Feedthrough Adapters
   * Connectors RECEIVED.
  * SR machining test ONGOING.
  * Installation stuff
   * "Ceiling" work in BS clean booth (removal of second floor section) scheduled for Fri 7/1.
   * Assembly frame construction scheduled for 7/4
  * Ballast masses for payload
   * Initial batch received - ordered extra smaller ones to allow for adjustments.
  * Lower breadboard stuff
   * Installation to be incorporated into the procedure document. Mark/Takahashi to discuss.
   * Breadboard springs (in manufacture, expected end of July)
   * Nail-head parts - ordered with assembly frame, will arrive next week.
  * Documents
   * BS Assembly Procedure [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=4235| E1504235]], [[https://onedrive.live.com/redir?resid=D5CCFA70A378E0D0!195&authkey=!AM_usynuo9QI57g&ithint=folder,webloc|E1504235 draft]]
=== Type B (Mark) ===
==== Report for week of 5/7 ====
 * We inspected the wires and clamps involved in the wire break.
  * The scars on the clamp on the tungsten wire that failed had very different depths, with the one that failed being much deeper, so probably the clamp piece was not completely straight before tensioning. However one wire on the other side was also badly crushed and on the point of failing, so the tension was clearly too much.
  * We decided on new torque specs of 2 N.m for the primary clamps (down from 5 N.m) and 10 N.m (down from 20 N.m) for the secondary. The secondary clamp spec, for M6 screws, is now based on the LIGO policy of using the maximum suggested for the screw and the LIGO value for a coated 1/4-20 screw (100 in-lb = 11.3 N.m), and the primary clamp spec is derated by 2/3 from the spec for an M5 screw because the clamp pieces are recessed and only grip the wire at narrow sections along the edges, concentrating the force.
  * None of the screws showed any signs of damage.
  * All of the scars on the primary clamps were shallow enough that could reuse the clamp pieces. The tungsten secondary clamps were never tightened, and the outer pieces of piano wire secondary clamps were badly scarred but could be reused upside down.
 * We successfully rehung the SR3 and RM. In the process we noticed and fixed an issue with the assembly frame (due to an out-of-date number in the Mirapro diagram, the IM crossbars were set 3 mm too high, which would have affected the wire length).
 * We added the sections of the security structure below the RM and up to the BF.
 * We installed the TM OSEM cables and routed them up to the IM.
 * We installed the load gauge adapter and load gauge and prepared the IM/... section for weighing.
 * We removed the three cracked F0 blades from the PI #3 in the SRM, and prepared for testing prototype new blades in that PI. We removed a floor panel under the PI and set up the filter service trolley underneath it with a stack of masses for a dummy load.

==== Plan for week of 5/14 ====
 * Mark, Enzo, Hirata-san, Kozu-kun at Kamioka Mon-Thu, then Osaka.
 *

==== Plan for week of 5/21 ====
 * Mark, Enzo, Hirata-san, Kamioka Mon-Fri.
 * Kozu-kun at Kamioka Wed-Fri.

==== Plan for week of 5/28 ====
 * Mark, Enzo, Hirata-san, Kamioka Mon-Fri.
 * Kozu-kun at Kamioka Mon only.
 
==== To-Do Lists, Schedule ====
 * [[KAGRA/Subgroups/VIS/TypeB/March2018]]
 * [[KAGRA/Subgroups/VIS/TypeB/April2018]]
 * [[KAGRA/Subgroups/VIS/TypeB/ToDoBS]]
 * [[KAGRA/Subgroups/VIS/TypeB/ToDoSR]]
 * [[https://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=7779|JGW-L1807779-v1 Type B Schedule (SR)]]

==== Vacation Info ====

Scraps of text for incorporation in the VIS Meeting Minutes

KAGRA/Subgroups/VIS/MeetingNAOJ

Type B (Mark)

Report for week of 5/7

  • We inspected the wires and clamps involved in the wire break.
    • The scars on the clamp on the tungsten wire that failed had very different depths, with the one that failed being much deeper, so probably the clamp piece was not completely straight before tensioning. However one wire on the other side was also badly crushed and on the point of failing, so the tension was clearly too much.
    • We decided on new torque specs of 2 N.m for the primary clamps (down from 5 N.m) and 10 N.m (down from 20 N.m) for the secondary. The secondary clamp spec, for M6 screws, is now based on the LIGO policy of using the maximum suggested for the screw and the LIGO value for a coated 1/4-20 screw (100 in-lb = 11.3 N.m), and the primary clamp spec is derated by 2/3 from the spec for an M5 screw because the clamp pieces are recessed and only grip the wire at narrow sections along the edges, concentrating the force.
    • None of the screws showed any signs of damage.
    • All of the scars on the primary clamps were shallow enough that could reuse the clamp pieces. The tungsten secondary clamps were never tightened, and the outer pieces of piano wire secondary clamps were badly scarred but could be reused upside down.
  • We successfully rehung the SR3 and RM. In the process we noticed and fixed an issue with the assembly frame (due to an out-of-date number in the Mirapro diagram, the IM crossbars were set 3 mm too high, which would have affected the wire length).
  • We added the sections of the security structure below the RM and up to the BF.
  • We installed the TM OSEM cables and routed them up to the IM.
  • We installed the load gauge adapter and load gauge and prepared the IM/... section for weighing.
  • We removed the three cracked F0 blades from the PI #3 in the SRM, and prepared for testing prototype new blades in that PI. We removed a floor panel under the PI and set up the filter service trolley underneath it with a stack of masses for a dummy load.

Plan for week of 5/14

  • Mark, Enzo, Hirata-san, Kozu-kun at Kamioka Mon-Thu, then Osaka.

Plan for week of 5/21

  • Mark, Enzo, Hirata-san, Kamioka Mon-Fri.
  • Kozu-kun at Kamioka Wed-Fri.

Plan for week of 5/28

  • Mark, Enzo, Hirata-san, Kamioka Mon-Fri.
  • Kozu-kun at Kamioka Mon only.

To-Do Lists, Schedule

Vacation Info

KAGRA/Subgroups/VIS/TypeB/Minutes (last edited 2022-10-28 10:02:46 by fabian.arellano)