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Revision 68 as of 2016-09-29 13:47:43
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Revision 157 as of 2017-06-15 16:21:47
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 * Type B Past Week Summary, weeks of 9/19 and 9/26
  * Fabian, Mark and Kuwahara-kun did BS installation at Kamioka:
   * The BS clean booth was modified 9/20-21 to allow crane access. The area was fairly clean when Fabian inspected it on 9/26, but there were lots of metal flakes stuck to tape holding foil over the slit in the top of the clean bag.
   * Mark created a new Type B rtcds model and MEDM screens for the BS, adapting the TypeBb/PR3.
   * Mark and Kokeyama-san debugged the new model, fixing several issues.
   * Kuwahara-kun derived OSEM2EUL and EUL2OSEM matrices.
   * Mark set up OSEMINF filters using measured OSEM calibration data to return outputs in µm.
   * Mark took free-swing data on the TM stage to get the pendulum mode frequencies for comparison to the SUMCON model.
   * Mark and Fabian debugged the coil output to the OSEMs. (At first the coil drive was not giving output because it did not have BIO inputs and so was reading the test input, not the main input. And for a while output failed because of a loose cable to the sat amp.)
   * Mark took fixed-sine TFs to check the polarity of the coil-magnet combinations.
  * Hirata-san:
   * Finished 3D CAD of SRM in tanks (but some work was lost due to a hard disk crash).
   * Did 3D and 2D for new maraging rods, stub flags for PR/SR (ditto re hard disk).
   * Measured/tested Type A BF #8 and started assembling #9.
 * Longer term to-do list
  * Do Inventor assembly for SRx in chamber and on assembly frame (Hirata) - SR2/SR3 DONE, SRM ongoing.
   * Part "disk security" top has to be modified - screw positions do not match.
  * Write more of payload assembly procedure (Fabian) - ONGOING
  * Write more of BS Assembly Procedure [[http://gwdoc.icrr.u-tokyo.ac.jp/cgi-bin/private/DocDB/ShowDocument?docid=4235| E1504235]], [[https://onedrive.live.com/redir?resid=D5CCFA70A378E0D0!195&authkey=!AM_usynuo9QI57g&ithint=folder,webloc|E1504235 draft]] (Mark) - ONGOING
  * Lower breadboard installation to be incorporated into the procedure document.
  * Work on BS simulation (Fabian)
  * Do BS Simulink model (Mark, Kokeyama) - TM/IM/BF level DONE
  * Do 2D drawings of SR2 parts (Hirata)
  * Redesign SRx IM wire clamps for larger prisms, remachined RMs
  * Order SRM/PRM parts (Hirata/Shoda)
  * Order SRx fasteners (Hirata)
=== Type B (Mark) ===
==== Past week report ====
At Kamioka (Mark, Fabian, Enzo, Hirata-san):
 * Hirata-san and Sekine-san moved the tank lid and service port ring to the pallet with the crane and covered the open tank with the spare clean bag.
 * Hirata-san and Mark got the LBB damper rings assembled and installed. A joint part for the Cu ring needed to have holes enlarged because the hole pattern did not quite match that on the half-ring. The magnet ring is hanging in the chamber and the Cu ring is attached below it with clamps, ready to receive the rods that will hang down from the PI.
 * Hirata-san recounted all the unused cables.
 * Hirata-san installed the outrigger parts on the LBB, which will receive the rods coming down from the damper ring.
 * Enzo and Mark tested all the stepper motors.
 * Enzo and Mark debugged the PI horizontal LVDTs. One LVDT had a flaky connection and one card in the LVDT driver had three dead channels. Enzo created a fully working driver using parts from another driver that also had a faulty card.
 * Fabian adjusted the ballast mass on the SF to get good pitch/roll/vertical adjustment and attached it with screws.
 * Fabian set up the optical lever again (the PR2 team had repossessed the breadboard we had been using but Akutsu-san supplied another one).
 *
==== Plan for coming weeks ====
For more detail, see [[KAGRA/Subgroups/VIS/TypeB/ToDo]].
Line 32: Line 20:
  Week of 6/12:
 * Cabling:
  * Debug/fix PI vertical LVDTs #0 and #2.
  * Calibrate PI vertical LVDT.
  * Debug/fix geophone #1.
  * Set yoke on PI vertical LVDT (if necessary).
  * Cable and test PI yaw stepper.
  * Cable and test PI vertical stepper.
  * Cable and test PI horizontal steppers.
  * Cable and test PI horizontal LVDTs.
  * Calibrate PI horizontal LVDTs.
 * Prepare LBB.
  * Attach LBB outriggers and rod receptacles.
 * Prepare LBB Cu ring.
  * Remove from tank, fix incompletely threaded holes, reinstall in tank.
  * Lay down spacers to protect magnets (in next step).
 * Prepare LBB magnet ring.
  * Disassemble.
  * Pass pieces into tank.
  * Reassemble on top of Cu ring.
 * Install LBB damper.
  * Bind LBB damper rings together with slings.
  * Remove vacuum tank lid and ring.
  * Crane rings up to install height, hook LBB magnet ring and support LBB Cu ring by TBD method.
 * Crane suspension into tank.
 * Hook LBB Cu ring.
 * Hook LBB.
 * Crane vacuum tank lid+ring black on.
 * Remove vacuum tank lid (only).
 * Remove port covers where feedthroughs will go, move feedthroughs from assembly frame and install on vacuum tank ring.
 * Reconnect in-air cables.

Scraps of text for incorporation in the VIS Meeting Minutes

KAGRA/Subgroups/VIS/MeetingNAOJ

Type B (Mark)

Past week report

At Kamioka (Mark, Fabian, Enzo, Hirata-san):

  • Hirata-san and Sekine-san moved the tank lid and service port ring to the pallet with the crane and covered the open tank with the spare clean bag.
  • Hirata-san and Mark got the LBB damper rings assembled and installed. A joint part for the Cu ring needed to have holes enlarged because the hole pattern did not quite match that on the half-ring. The magnet ring is hanging in the chamber and the Cu ring is attached below it with clamps, ready to receive the rods that will hang down from the PI.
  • Hirata-san recounted all the unused cables.
  • Hirata-san installed the outrigger parts on the LBB, which will receive the rods coming down from the damper ring.
  • Enzo and Mark tested all the stepper motors.
  • Enzo and Mark debugged the PI horizontal LVDTs. One LVDT had a flaky connection and one card in the LVDT driver had three dead channels. Enzo created a fully working driver using parts from another driver that also had a faulty card.
  • Fabian adjusted the ballast mass on the SF to get good pitch/roll/vertical adjustment and attached it with screws.
  • Fabian set up the optical lever again (the PR2 team had repossessed the breadboard we had been using but Akutsu-san supplied another one).

Plan for coming weeks

For more detail, see KAGRA/Subgroups/VIS/TypeB/ToDo.

Week of 6/12:

  • Cabling:
    • Debug/fix PI vertical LVDTs #0 and #2.
    • Calibrate PI vertical LVDT.
    • Debug/fix geophone #1.
    • Set yoke on PI vertical LVDT (if necessary).
    • Cable and test PI yaw stepper.
    • Cable and test PI vertical stepper.
    • Cable and test PI horizontal steppers.
    • Cable and test PI horizontal LVDTs.
    • Calibrate PI horizontal LVDTs.
  • Prepare LBB.
    • Attach LBB outriggers and rod receptacles.
  • Prepare LBB Cu ring.
    • Remove from tank, fix incompletely threaded holes, reinstall in tank.
    • Lay down spacers to protect magnets (in next step).
  • Prepare LBB magnet ring.
    • Disassemble.
    • Pass pieces into tank.
    • Reassemble on top of Cu ring.
  • Install LBB damper.
    • Bind LBB damper rings together with slings.
    • Remove vacuum tank lid and ring.
    • Crane rings up to install height, hook LBB magnet ring and support LBB Cu ring by TBD method.
  • Crane suspension into tank.
  • Hook LBB Cu ring.
  • Hook LBB.
  • Crane vacuum tank lid+ring black on.
  • Remove vacuum tank lid (only).
  • Remove port covers where feedthroughs will go, move feedthroughs from assembly frame and install on vacuum tank ring.
  • Reconnect in-air cables.

KAGRA/Subgroups/VIS/TypeB/Minutes (last edited 2022-10-28 10:02:46 by fabian.arellano)