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Revision 79 as of 2016-10-27 12:56:30
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Revision 84 as of 2016-11-18 13:54:10
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Editor: MarkBarton
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  * Fabian, Mark and Liu-kun did BS installation at Kamioka:
   * Debugged the issue with the BF keystone being tilted enough to cause rubbing on the yoke for the magnets. It was solved by moving the yoke ≈1 mm taking advantage of the oversized holes.
   * Measured the height of the payload as a function of trim mass. The BF spring seems to have a slightly lower load capacity and a rather higher spring constant than when it was remeasured by Hirata-san.
   * Removed IM trim mass to set the average height of the keystone to the CAD value.
   * Moved IM trim mass around to set the pitch of the dummy BS.
  * Hirata-san
   * TBD.
 
  * Mark and Hirata-san worked at Kamioka, with valuable help from Enzo (on loan from Type Bp team).
  * We got all the adapter cables for the BF made (Hirata-san did some work on Monday at Mitaka).
  * We installed the extension for the BF yaw pico on the IM pico adapter cable.
  * We got all the in-vacuum and in-air cabling for the IM OSEMs done.
  * We tried to install the stepper and LVDT adapter cables but realized we didn't have enough information on which wires was which. (We later tracked this info down but did not have time to do anything with it - we would have needed to do the rest of the in-vacuum and in-air cabling and set up the stepper motor and LVDT drivers, so we concentrated on the OSEMs.)
  * We plugged in the IM OSEMs, set gains and offsets, and did a noise test (analysis and klog pending).
  * We mounted the OSEMs on the IRM and routed the cabling neatly.
  * We released the suspension.
  * We adjusted the OSEM mounting plates to center the OSEMs on the flags.
  * We adjusted the OSEMs in/out to midrange.
  * The suspension is now ready for OSEM-OSEM TFs!

Scraps of text for incorporation in the VIS Meeting Minutes

KAGRA/Subgroups/VIS/MeetingNAOJ

  • Type B Past Week Summary
    • Mark and Hirata-san worked at Kamioka, with valuable help from Enzo (on loan from Type Bp team).
    • We got all the adapter cables for the BF made (Hirata-san did some work on Monday at Mitaka).
    • We installed the extension for the BF yaw pico on the IM pico adapter cable.
    • We got all the in-vacuum and in-air cabling for the IM OSEMs done.
    • We tried to install the stepper and LVDT adapter cables but realized we didn't have enough information on which wires was which. (We later tracked this info down but did not have time to do anything with it - we would have needed to do the rest of the in-vacuum and in-air cabling and set up the stepper motor and LVDT drivers, so we concentrated on the OSEMs.)
    • We plugged in the IM OSEMs, set gains and offsets, and did a noise test (analysis and klog pending).
    • We mounted the OSEMs on the IRM and routed the cabling neatly.
    • We released the suspension.
    • We adjusted the OSEM mounting plates to center the OSEMs on the flags.
    • We adjusted the OSEMs in/out to midrange.
    • The suspension is now ready for OSEM-OSEM TFs!

KAGRA/Subgroups/VIS/TypeB/Minutes (last edited 2022-10-28 10:02:46 by fabian.arellano)