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 * Hirata-san produced a near-final Inventor assembly of the BS on the assembly frame, for use in writing the assembly procedure.
  * Includes assembly frame modifications suggested by Mirapro, including feet, wheels, lifting eyes, thicker crossbars under BF, IM etc.
  * Includes final rail system except for interface plate to mirror box.
  * Includes full PI with ballast masses.
  * Includes cable clamps.
  * Includes correct versions of BF and SF.
  * Includes new BF pushrod parts to work around different placement of blade screws in new version of BF.
  * Includes cleanbag support bars.
  * Includes key parts of mirror box (enough to check for interference) - needs more work.
  * Does not include various invisible duplicate assemblies that had been present due to cut and paste.
  * After a few more improvements, the new assembly will be sent back to Mirapro.
 * Got status from Miyakawa-san on electronics - there should be enough of the boxes AEL is supplying.
 * Cleanbag design was finalized; Aso-san is ordering: [[attachment:160419-チャンバーカバーⅡ型.pdf]]
 * Quote for flags and prisms was received, but expensive - may drop rigid flag design.
 * The mirror box will require only very minor modifications for flags and prisms - Tatsumi-san will arrange immediately.
 * Fabian worked on understanding Sekiguchi-san's control design to help decide optimum wire thickness.
 * Mark worked on install procedure and schedule.
 * Takahashi-san enquired with NIKHEF about oscillator cards for LVDT chassis - lead time would be 3-4 months.
 *
=== Type B (Mark) ===
==== Report for week of 1/15 ====
 * We swapped in the other available BF, and it was rather better: only 0.3 mm of keystone tilt rather than 1.3 mm. We will use it for the SR2 and then think about whether we want to use or rebuild the original one.
 * We finished the preparation of the second BF, setting the yoke, adding the new-style cable clamps etc.
 * We changed the 1.6 mm sockets on the BF LVDT cable to 1.0 mm ones to match the pins on the LVDT wires. The specification of the cable in D1503901 was apparently wrong. We will update it (today) before doing the cable order for the SR3 and SRM.
 * We received, unpacked and temporarily stored a shipment of weights and other parts that will be used to check the load capacity of the top filters.
 * We updated the BS real-time model and screens, adding support for a damping filter common to both the OL-TM and OL-IM paths, per Izumi-san's suggestion in G1807653.
 * We set up the router for the SR2 rack and got the SR2_IM pico driver and both stepper motors on the network (the SR2_BF pico is still on order).
 

==== Plan for week of 1/29 ====
 * Enzo at Mitaka 1/29 and most of 1/30, then vacation.
 * Kozu-kun away.
 * All others at Kamioka.
 * Test IM picos and BF yaw pico.
 * Calibrate LVDT.
 * Install ballast mass in BF.
 * Build IRM around IM.
 * Cable/test/adjust IM OSEMs.
 * Time permitting, do TFs from IM OSEMs to themselves and to optical sensor.

==== Vacation Info ====
 * Enzo 1/30-2/19 (at Mitaka 1/29, part of 1/30)
 * Kozu-kun 1/29-2/2

Scraps of text for incorporation in the VIS Meeting Minutes

KAGRA/Subgroups/VIS/MeetingNAOJ

Type B (Mark)

Report for week of 1/15

  • We swapped in the other available BF, and it was rather better: only 0.3 mm of keystone tilt rather than 1.3 mm. We will use it for the SR2 and then think about whether we want to use or rebuild the original one.
  • We finished the preparation of the second BF, setting the yoke, adding the new-style cable clamps etc.
  • We changed the 1.6 mm sockets on the BF LVDT cable to 1.0 mm ones to match the pins on the LVDT wires. The specification of the cable in D1503901 was apparently wrong. We will update it (today) before doing the cable order for the SR3 and SRM.
  • We received, unpacked and temporarily stored a shipment of weights and other parts that will be used to check the load capacity of the top filters.
  • We updated the BS real-time model and screens, adding support for a damping filter common to both the OL-TM and OL-IM paths, per Izumi-san's suggestion in G1807653.
  • We set up the router for the SR2 rack and got the SR2_IM pico driver and both stepper motors on the network (the SR2_BF pico is still on order).

Plan for week of 1/29

  • Enzo at Mitaka 1/29 and most of 1/30, then vacation.
  • Kozu-kun away.
  • All others at Kamioka.
  • Test IM picos and BF yaw pico.
  • Calibrate LVDT.
  • Install ballast mass in BF.
  • Build IRM around IM.
  • Cable/test/adjust IM OSEMs.
  • Time permitting, do TFs from IM OSEMs to themselves and to optical sensor.

Vacation Info

  • Enzo 1/30-2/19 (at Mitaka 1/29, part of 1/30)
  • Kozu-kun 1/29-2/2

KAGRA/Subgroups/VIS/TypeB/Minutes (last edited 2022-10-28 10:02:46 by fabian.arellano)