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* Type B Past Week Summary * Mark (with Enzo) did initial TFs on the BF. * Did fixed-sine TFs on individual OSEMs at low frequency to check actuator polarity (klog [[http://klog.icrr.u-tokyo.ac.jp/osl/?r=2176 | 2176]] and [[http://klog.icrr.u-tokyo.ac.jp/osl/?r=2182|2182]]). * Set gains in the COILOUTF block to compensate for actuator polarity. * Mark (with Enzo) did a free-swing measurement on the BS after earthquake of 11/22 (klog [[http://klog.icrr.u-tokyo.ac.jp/osl/?r=2182|2182]]). * Results suspicious (noted by Shoda-san): too much difference between OSEMs - horizontal showing much less motion than vertical. * Possible rubbing in horizontal. * May need a trip to Kamioka. * Mark (with Enzo) made corrections and improvements to many of the MEDM screens (klog [[http://klog.icrr.u-tokyo.ac.jp/osl/?r=2176 | 2176]] and [[http://klog.icrr.u-tokyo.ac.jp/osl/?r=2182|2182]]). * Main overview screen was not generic in many places, and links to GDS_TP screens were broken. * ADC monitor screen referenced bad channels with LIGO-style names. * DAC monitor screen was not generic and did not support IM OSEMs. * Watchdog IM OSEM AC band limit filter screen was a copy of the TM one. * Watchdog TM OSEM AC band limit filter screen appears to be getting OL signals as input - needs model changes to fix. * The zoomed screens for IM OSEM centering were called incorrectly and did not work. * Various screens had LIGO-style channel names as labels. * Mark did a draft of D1603600-v12 reflecting the new assignment of IM OSEMs to DAQ channels (#4-9 are now V1, V2, V3, H1, H2, H3 rather than H1, H2, ...) from last Friday (the wiring was changed to reflect the model). * Mark worked on schedule. * Hirata-san |
* Mark, Fabian and Enzo continued BS Test Hang work: * We installed the BF fishing rod stepper motor adaptor cable. * We tried to install the BF LVDT cable but first we encountered trouble routing it, and then several wires broke at the D-Sub end. * We laid 6 in-air cables from the tank to the PR2 rank for BF and SF picos, steppers and LVDTs. * We lifted the BF/IRM/IM/RM/BS section to weigh it and check its balance. * It was 195.6 kg, which is 18 kg(!) less than the capacity of the SF. * There was a major imbalance in roll: with all four built-in trim masses moved up the +Y end, it still needed 270 g of extra trim mass to be level. * Unfortunately when we put the payload, the IM was slightly yawed and ended up on the horizontal EQ stop screws. This let the IM-BF maraging rod go slack, which disturbed the leveling of the IM (because every time it is picked up the maraging rod settles in a different place, giving a different suspension point). We may have to partly disassemble the IRM and rearrange the time mass on the the IM. * We shipped BS mirror box parts to Shoda-san and components for a new LVDT cable to Hirata-san. * We posed for pictures of the BS by a team from National Geographic. * Hirata-san * Did parts and fastener lists for the SR payload. * Did a 3D model with the SR suspension on the BS assembly frame (to help Mark make adjustments to the frame design). * Did 2D drawings of Fabian's concept for BS EQ stop parts. * Did a 3D model of a wire clamp with replaceable jaw parts (to avoid having to reuse parts with scars from pressure). * Did 2D drawings of a new wire clamps for on top of the BS and SR RMs. |
Scraps of text for incorporation in the VIS Meeting Minutes
KAGRA/Subgroups/VIS/MeetingNAOJ
- Mark, Fabian and Enzo continued BS Test Hang work:
- We installed the BF fishing rod stepper motor adaptor cable.
- We tried to install the BF LVDT cable but first we encountered trouble routing it, and then several wires broke at the D-Sub end.
- We laid 6 in-air cables from the tank to the PR2 rank for BF and SF picos, steppers and LVDTs.
- We lifted the BF/IRM/IM/RM/BS section to weigh it and check its balance.
- It was 195.6 kg, which is 18 kg(!) less than the capacity of the SF.
- There was a major imbalance in roll: with all four built-in trim masses moved up the +Y end, it still needed 270 g of extra trim mass to be level.
- Unfortunately when we put the payload, the IM was slightly yawed and ended up on the horizontal EQ stop screws. This let the IM-BF maraging rod go slack, which disturbed the leveling of the IM (because every time it is picked up the maraging rod settles in a different place, giving a different suspension point). We may have to partly disassemble the IRM and rearrange the time mass on the the IM.
- We shipped BS mirror box parts to Shoda-san and components for a new LVDT cable to Hirata-san.
- We posed for pictures of the BS by a team from National Geographic.
- Hirata-san
- Did parts and fastener lists for the SR payload.
- Did a 3D model with the SR suspension on the BS assembly frame (to help Mark make adjustments to the frame design).
- Did 2D drawings of Fabian's concept for BS EQ stop parts.
- Did a 3D model of a wire clamp with replaceable jaw parts (to avoid having to reuse parts with scars from pressure).
- Did 2D drawings of a new wire clamps for on top of the BS and SR RMs.