Differences between revisions 86 and 98 (spanning 12 versions)
Revision 86 as of 2016-11-25 10:37:25
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Revision 98 as of 2016-12-16 09:33:25
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Editor: MarkBarton
Comment:
Deletions are marked like this. Additions are marked like this.
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 * Type B Past Week Summary
  * Mark (with Enzo) did initial TFs on the BF.
   * Did fixed-sine TFs on individual OSEMs at low frequency to check actuator polarity (klog [[http://klog.icrr.u-tokyo.ac.jp/osl/?r=2176 | 2176]] and [[http://klog.icrr.u-tokyo.ac.jp/osl/?r=2182|2182]]).
   * Set gains in the COILOUTF block to compensate for actuator polarity.
  * Mark (with Enzo) did a free-swing measurement on the BS after earthquake of 11/22 (klog [[http://klog.icrr.u-tokyo.ac.jp/osl/?r=2182|2182]]).
   * Results suspicious (noted by Shoda-san): too much difference between OSEMs - horizontal showing much less motion than vertical.
   * Possible rubbing in horizontal.
   * May need a trip to Kamioka.
  * Mark (with Enzo) made corrections and improvements to many of the MEDM screens (klog [[http://klog.icrr.u-tokyo.ac.jp/osl/?r=2176 | 2176]] and [[http://klog.icrr.u-tokyo.ac.jp/osl/?r=2182|2182]]).
   * Main overview screen was not generic in many places, and links to GDS_TP screens were broken.
   * ADC monitor screen referenced bad channels with LIGO-style names.
   * DAC monitor screen was not generic and did not support IM OSEMs.
   * Watchdog IM OSEM AC band limit filter screen was a copy of the TM one.
   * Watchdog TM OSEM AC band limit filter screen appears to be getting OL signals as input - needs model changes to fix.
   * The zoomed screens for IM OSEM centering were called incorrectly and did not work.
   * Various screens had LIGO-style channel names as labels.
  * Mark did a draft of D1603600-v12, including:
   * New assignment of IM OSEMs to DAQ channels (#4-9 are now V1, V2, V3, H1, H2, H3 rather than H1, H2, ...) from last Friday (the wiring was changed to reflect the model).
   * Information on how to identify the wires from the steppers and LVDTs so that the adapter cables can be plugged in properly.
  * Mark worked on schedule.
  * Hirata-san did drawings for new 8-mm maraging wires for Type A.
  * Hirata-san worked on PR/SR mirror box modifications with Shoda-san.
  
 * Mark, Fabian and Enzo continued BS Test Hang work:
  * We shipped BS mirror box parts to Shoda-san and components for a new LVDT cable to Hirata-san.
  * We posed for pictures of the BS by a team from National Geographic.
  * We installed the BF fishing rod stepper motor adaptor cable.
  * We tried to install the BF LVDT cable but first we encountered trouble routing it, and then several wires broke at the D-Sub end.
  * We laid 6 in-air cables from the tank to the PR2 rank for BF and SF picos, steppers and LVDTs.
  * We lifted the BF/IRM/IM/RM/BS section to weigh it and check its balance.
   * It was 195.6 kg, which is 18 kg(!) less than the capacity of the SF.
   * There was a major imbalance in roll: with all four built-in trim masses moved up the +Y end, it still needed 270 g of extra trim mass to be level. This can probably be made up easily by designing the 18 kg of extra mass appropriately.
  * Unfortunately when we put the payload, the IM was slightly yawed and ended up on the horizontal EQ stop screws. This let the IM-BF maraging rod go slack, which disturbed the leveling of the IM (because every time it is picked up the maraging rod settles in a different place, giving a different suspension point).
  * We removed the end panels of the IRM to get access to the IM and rearranged the trim mass on the the IM to get it balance to bubble-level precision. (We still need to do fine pitch adjustment with the OL so that the BS is at the right angle, secure the trim mass properly and replace the IRM panels and OSEMs.)
 * Miyakawa-san and Yamamoto-san redid the cabling from the computer room to the PR2 rack and expected to finish by lunchtime on Friday.
 * Hirata-san
  * Did parts and fastener lists for the SR payload.
  * Did a 3D model with the SR suspension on the BS assembly frame (to help Mark make adjustments to the frame design).
  * Did 2D drawings of Fabian's concept for BS EQ stop parts.
  * Did a 3D model of a wire clamp with replaceable jaw parts (to avoid having to reuse parts with scars from pressure).
  * Did 2D drawings of a new wire clamps for on top of the BS and SR RMs.

Scraps of text for incorporation in the VIS Meeting Minutes

KAGRA/Subgroups/VIS/MeetingNAOJ

  • Mark, Fabian and Enzo continued BS Test Hang work:
    • We shipped BS mirror box parts to Shoda-san and components for a new LVDT cable to Hirata-san.
    • We posed for pictures of the BS by a team from National Geographic.
    • We installed the BF fishing rod stepper motor adaptor cable.
    • We tried to install the BF LVDT cable but first we encountered trouble routing it, and then several wires broke at the D-Sub end.
    • We laid 6 in-air cables from the tank to the PR2 rank for BF and SF picos, steppers and LVDTs.
    • We lifted the BF/IRM/IM/RM/BS section to weigh it and check its balance.
      • It was 195.6 kg, which is 18 kg(!) less than the capacity of the SF.
      • There was a major imbalance in roll: with all four built-in trim masses moved up the +Y end, it still needed 270 g of extra trim mass to be level. This can probably be made up easily by designing the 18 kg of extra mass appropriately.
    • Unfortunately when we put the payload, the IM was slightly yawed and ended up on the horizontal EQ stop screws. This let the IM-BF maraging rod go slack, which disturbed the leveling of the IM (because every time it is picked up the maraging rod settles in a different place, giving a different suspension point).
    • We removed the end panels of the IRM to get access to the IM and rearranged the trim mass on the the IM to get it balance to bubble-level precision. (We still need to do fine pitch adjustment with the OL so that the BS is at the right angle, secure the trim mass properly and replace the IRM panels and OSEMs.)
  • Miyakawa-san and Yamamoto-san redid the cabling from the computer room to the PR2 rack and expected to finish by lunchtime on Friday.
  • Hirata-san
    • Did parts and fastener lists for the SR payload.
    • Did a 3D model with the SR suspension on the BS assembly frame (to help Mark make adjustments to the frame design).
    • Did 2D drawings of Fabian's concept for BS EQ stop parts.
    • Did a 3D model of a wire clamp with replaceable jaw parts (to avoid having to reuse parts with scars from pressure).
    • Did 2D drawings of a new wire clamps for on top of the BS and SR RMs.

KAGRA/Subgroups/VIS/TypeB/Minutes (last edited 2022-10-28 10:02:46 by fabian.arellano)