Differences between revisions 5 and 15 (spanning 10 versions)
Revision 5 as of 2017-01-25 14:58:58
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Editor: YoichiAso
Comment:
Revision 15 as of 2017-01-27 20:06:09
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Editor: NaokoOhishi
Comment:
Deletions are marked like this. Additions are marked like this.
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Participants: Participants: Tanaka, Mark, Sato, Ishizaki, Fabian, Hirata, Okutomi, Shoda, Enzo, Someya, Hashimoto, Akutsu
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 * Put a report here  * [[http://gwwiki.icrr.u-tokyo.ac.jp/JGWwiki/KAGRA/Subgroups/VIS/TypeA/Meeting|Minutes of Type-A Meeting]]
 * EYV chamber: Top chamber was connected again.
 * Pre-isolator: The pre-isolators for SR were packed and moved out of the large clean room on 23rd.
 * BF damper: Checked delivered parts on 24th.
 * Maraging wire: The wires are delivered on 31st. They are sent to the thermal proccess on 1st February. To be shipped to Kamioka on Feb. 7th.
  The 3.3m wire can be treated at Himeji facility of Kinzoku-giken.
 * Preparation of installation: The floor of clean booth was covered by stainless steel sheet. The foot holds were assembled.
  Other large tools (rack, wagon, desk, so on) also were installed into the clean booth.

 Next Week Plan

 * BF damping pre-assembly
 * Open the top chamber.
 * Set the assembly base.
 * Sato-san will stay in Mitaka to send the delivered rods to the heat treatment. Also incorporate cables into the Type-A CAD model.
Line 15: Line 29:
 * Put a report here  * Hirata-san:
  * Received many parts from i-ject for BFRM (took pictures and took them into ATC cleanroom).
  * Got quotes for PRM/SRM payload from i-ject.
  * Checked quotes and asked for some modifications.)
  * Washed parts (parts for type-A, small hexagons, screws, etc\)
  * Wiped 9 piano wires and sent to Kamioka for PR.
  * Updated Fabian's EQstop parts for BS recoilmass and updated EQstop assy drawings.
 * Fabian
  * Worked out geometry for blade adjustment.
  * Designed additional ballast masses for BS BF (and SR).
 * Mark and Enzo (at Kamioka)
  * Did two rounds of adjustment of the blades with help from Takahashi-san (one for position, one for frequency)
  * Surveyed the position of the rod using the vertical mode of the bubble level.
  * Got apparent improvement as judged at the IRM-IM EQ stops (but still not perfect).
  * Did one more round of blade adjustments (without Takahashi-san)
  * Got good agreement with IRM-IM EQ stops, so put BF cap on and raised the whole system to check for balance.
  * Found balance still fairly bad: about the same on the -X,+Y diagonal and about half on the +X,+Y diagonal (70 and 30 mm worth of motion of a single trim mass respectively; previous a bit over 70 mm each). Moreover, IRM-IM alignment no longer good.
  * From the imbalance torques, calculated the offset of rod as 2.3 mm in the direction 22 degrees to the +X side of -Y.
  * Calculated the blade adjustments required: {-0.325194, -1.79175, 2.11695} mm
  * Prepared to apply adjustments (removed cap etc).
=== Type-Bp (Shoda) ===
 * '''Hanging Report''': TF measured, BF has been set.
  * EQ stop parts below the BF were assembled.
  * We measured TFs of RM using PSs. (Their alignment was not so easy.)
  * BF was placed on the EQ stop. (Traverser was moved out of the clean room for accesibility.)
  * BF and IM was connected. Not hanged yet.
  * BFRM parts were delivered.
   * Test assemble them in Mitaka on Feb. 2nd.
Line 17: Line 58:
=== Type-Bp (Shoda) ===
 * Put a report here
 * '''Next week task''': Hang IRM
  * Hang IM and adjust the weight.
  * Hang IRM and balance IM.
  * IRM and set OSEMs.
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 * A mirror box was sent to a company for modification
 * Flag bases were sent to a company for modification
 * Winch were sent to Mitaka for inspection

 * '''To do'''
  * Establish disassemble procedure
  * Buy the new tools
Line 21: Line 71:
 * Put a report here  * Last week we put IMMT mirrors in suspension.
 * This week, we have adjusted the mirror position and angle to be the same as old ones.
 * Beam profile measurement, which aims at adjusting the mirror position, was postponed to next week.
Line 24: Line 76:
 * Put a report here  * WDS PCB Design Document.Main rack( Main board + peripheral board )design.
   *Correction of PCB design and correction by DRC(by manufacturer).[[http://gwdoc.icrr.u-tokyo.ac.jp/DocDB/0061/E1706101/001/Project%20WDS%20PCB%20Design%20Ver1%28Detail%29170127.pdf|PDF(JGW-E1706101)]]
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 * Incidents:  * Incidents: cut finger with a stainless steel sheet
  * We need to wear globes for this kind of work

Type-A:
Type-B: Crane work to lift the BF up.
Type-Bp: No heavy lifting. Mirror does not move.
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  * Type-A:
  * Type-B:
  * Type-Bp:
  * Type-A: Open the top chamber (a crane work).
  * Type-B: Crane work to lift the BF up.
  * Type-Bp: No heavy lifting. Mirror does not move.
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  * We will use the same PEEK (Ketron CA30). This material was chosen to avoid charging.
Line 39: Line 99:
 * Mon:
 * Tue:
 * Wed:
 * Thu:
 * Fri:
 * Mon: BF blade adjustment (B)/Hang IM(Bp)
 * Tue: BF damper pre-assembly (A)/BF blade adjustment (B)/Assemble IMRM (Bp)
 * Wed: BF damper pre-assembly (A)/BF blade adjustment (B)/Assemble IMRM (Bp), Delivery of the parts for optical bench (Bp)
 * Thu: Open the chamber (A)/BF blade adjustment (B)
 * Fri: Set up assembly frame (A)/BF blade adjustment (B)
Line 48: Line 108:
  * Takahashi: 30-2/3
  * Shoda: 31-2/3
  * Takahashi: 31-2/3
  * Shoda: 30-2/1
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  * Fabian:   * Fabian: 30-2/3
Line 53: Line 113:
  * Fujii: 
  * Ishizaki: 30-2/3
  * Fujii:
  * Ishizaki: 31-2/3
Line 56: Line 116:
  * Sato: 30-2/3   * Sato:
Line 58: Line 118:
  * Hashimoto (Hosei Univ.):
  * Someya (Hosei Univ.): 
  * Hashimoto (Hosei Univ.): 30-2/1
  * Someya (Hosei Univ.):30-2/1
Line 63: Line 123:
  * Takahashi:
  * Shoda:
  * Mark:
  * Fabian:
  * Okutomi:
  * Takahashi: 6-10
  * Shoda: 6-10
  * Mark: 6-10
  * Fabian: 6-10
  * Okutomi: 6-10
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  * Ishizaki:
  * Hirata:
  * Sato:
  * Enzo:
  * Hashimoto (Hosei Univ.):
  * Someya (Hosei Univ.):
  * Ishizaki: 6-10
  * Hirata: 6-10
  * Sato: 6-10
  * Enzo: 6-10
  * Hashimoto (Hosei Univ.): 6-10
  * Someya (Hosei Univ.): 6-10
Line 80: Line 140:
March VIS F2F: March 10 ?

Agenda/Minutes of the VIS Meeting on 2017/1/27

2017/1/27 13:30 -

Participants: Tanaka, Mark, Sato, Ishizaki, Fabian, Hirata, Okutomi, Shoda, Enzo, Someya, Hashimoto, Akutsu

Progress report

Schedule Chart : (PDF,MPP)

Type-A (Takahashi)

  • Minutes of Type-A Meeting

  • EYV chamber: Top chamber was connected again.
  • Pre-isolator: The pre-isolators for SR were packed and moved out of the large clean room on 23rd.
  • BF damper: Checked delivered parts on 24th.
  • Maraging wire: The wires are delivered on 31st. They are sent to the thermal proccess on 1st February. To be shipped to Kamioka on Feb. 7th.
    • The 3.3m wire can be treated at Himeji facility of Kinzoku-giken.
  • Preparation of installation: The floor of clean booth was covered by stainless steel sheet. The foot holds were assembled.
    • Other large tools (rack, wagon, desk, so on) also were installed into the clean booth.
    Next Week Plan
  • BF damping pre-assembly
  • Open the top chamber.
  • Set the assembly base.
  • Sato-san will stay in Mitaka to send the delivered rods to the heat treatment. Also incorporate cables into the Type-A CAD model.

Type B (Mark)

  • Hirata-san:
    • Received many parts from i-ject for BFRM (took pictures and took them into ATC cleanroom).
    • Got quotes for PRM/SRM payload from i-ject.
    • Checked quotes and asked for some modifications.)
    • Washed parts (parts for type-A, small hexagons, screws, etc\)
    • Wiped 9 piano wires and sent to Kamioka for PR.
    • Updated Fabian's EQstop parts for BS recoilmass and updated EQstop assy drawings.
  • Fabian
    • Worked out geometry for blade adjustment.
    • Designed additional ballast masses for BS BF (and SR).
  • Mark and Enzo (at Kamioka)
    • Did two rounds of adjustment of the blades with help from Takahashi-san (one for position, one for frequency)
    • Surveyed the position of the rod using the vertical mode of the bubble level.
    • Got apparent improvement as judged at the IRM-IM EQ stops (but still not perfect).
    • Did one more round of blade adjustments (without Takahashi-san)
    • Got good agreement with IRM-IM EQ stops, so put BF cap on and raised the whole system to check for balance.
    • Found balance still fairly bad: about the same on the -X,+Y diagonal and about half on the +X,+Y diagonal (70 and 30 mm worth of motion of a single trim mass respectively; previous a bit over 70 mm each). Moreover, IRM-IM alignment no longer good.
    • From the imbalance torques, calculated the offset of rod as 2.3 mm in the direction 22 degrees to the +X side of -Y.
    • Calculated the blade adjustments required: {-0.325194, -1.79175, 2.11695} mm
    • Prepared to apply adjustments (removed cap etc).

Type-Bp (Shoda)

  • Hanging Report: TF measured, BF has been set.

    • EQ stop parts below the BF were assembled.
    • We measured TFs of RM using PSs. (Their alignment was not so easy.)
    • BF was placed on the EQ stop. (Traverser was moved out of the clean room for accesibility.)
    • BF and IM was connected. Not hanged yet.
    • BFRM parts were delivered.
      • Test assemble them in Mitaka on Feb. 2nd.
  • Next week task: Hang IRM

    • Hang IM and adjust the weight.
    • Hang IRM and balance IM.
    • IRM and set OSEMs.
  • A mirror box was sent to a company for modification
  • Flag bases were sent to a company for modification
  • Winch were sent to Mitaka for inspection
  • To do

    • Establish disassemble procedure
    • Buy the new tools

IMMT (Ohishi)

  • Last week we put IMMT mirrors in suspension.
  • This week, we have adjusted the mirror position and angle to be the same as old ones.
  • Beam profile measurement, which aims at adjusting the mirror position, was postponed to next week.

Watchdog system (Tanaka)

  • WDS PCB Design Document.Main rack( Main board + peripheral board )design.

Safety

  • Incidents: cut finger with a stainless steel sheet
    • We need to wear globes for this kind of work

Type-A: Type-B: Crane work to lift the BF up. Type-Bp: No heavy lifting. Mirror does not move.

  • Foreseen risks
    • Type-A: Open the top chamber (a crane work).
    • Type-B: Crane work to lift the BF up.
    • Type-Bp: No heavy lifting. Mirror does not move.

Discussion

  • Smaller coil design status update (Aso)
    • We will use the same PEEK (Ketron CA30). This material was chosen to avoid charging.

Site work plan for the next week

  • Mon: BF blade adjustment (B)/Hang IM(Bp)
  • Tue: BF damper pre-assembly (A)/BF blade adjustment (B)/Assemble IMRM (Bp)
  • Wed: BF damper pre-assembly (A)/BF blade adjustment (B)/Assemble IMRM (Bp), Delivery of the parts for optical bench (Bp)
  • Thu: Open the chamber (A)/BF blade adjustment (B)
  • Fri: Set up assembly frame (A)/BF blade adjustment (B)

Travel Plans

  • Travel (Week of 1/30):
    • Takahashi: 31-2/3
    • Shoda: 30-2/1
    • Mark: 30-2/3
    • Fabian: 30-2/3
    • Okutomi: 30-2/3
    • Fujii:
    • Ishizaki: 31-2/3
    • Hirata:
    • Sato:
    • Enzo: 30-2/3
    • Hashimoto (Hosei Univ.): 30-2/1
    • Someya (Hosei Univ.):30-2/1
    • Ohishi:
  • Travel (Week of 2/6):
    • Takahashi: 6-10
    • Shoda: 6-10
    • Mark: 6-10
    • Fabian: 6-10
    • Okutomi: 6-10
    • Fujii:
    • Ishizaki: 6-10
    • Hirata: 6-10
    • Sato: 6-10
    • Enzo: 6-10
    • Hashimoto (Hosei Univ.): 6-10
    • Someya (Hosei Univ.): 6-10
    • Ohishi:

Next meeting

On 2017/2/3(Fri) VIS F2F: Feb. 17th March VIS F2F: March 10 ?

KAGRA/Subgroups/VIS/VISMinutes20170127 (last edited 2017-01-27 20:06:09 by NaokoOhishi)