Size: 1398
Comment:
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Size: 3040
Comment:
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Deletions are marked like this. | Additions are marked like this. |
Line 8: | Line 8: |
Schedule Chart : ([[https://www.dropbox.com/s/rlnmlt3uipcsai8/VIS%20Overall%20Schedule-20170121.pdf?dl=0|PDF]],[[https://www.dropbox.com/s/rlnmlt3uipcsai8/VIS%20Overall%20Schedule-20170121.pdf?dl=0|MPP]]) | Schedule Chart : ([[https://www.dropbox.com/s/3fllgzwp4wlew2k/VIS%20Overall%20Schedule-20170322.pdf?dl=0|PDF]],[[https://www.dropbox.com/s/agsjc8jqo2t6vxu/VIS%20Overall%20Schedule-20170322.mpp?dl=0|MPP]]) |
Line 12: | Line 12: |
Installation in Y-end: 13th(Mon) * Assembled cables for PCV for the BF damper. * Started cabling between the BF and the F3. 14th(Tue) * Continued cabling between the BF and the F3. * All cables reached the EQ stop for F3. 15th(Wed) * Tuned the F3 after cabling. * The effective weight of cables was about 1kg. It was larger than our prediction. * Removed the ballast mass inside the BF. 16th(Thu) * Repaired the stepping motor driver and modified the release sensor monitor. 17th(Fri) * Assembled the end plate for F2. 21st(Tue) * Calibrated the LVDT of F3 using the digital system. * The keystone of BF was not working. 22nd(Wed) * Took the F2 from the box and moved it into the clean booth. * Lifted up the DP stage and adjusted the weight of DP. 23rd(Thu) * Lifted down the BF stage into the corrugate tube. * The position of keystone on the F3 was too high. * The cable cramp on the bottom of BF was hitting the release sensor. * Adjusted the yaw rotation of BF. |
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Line 13: | Line 42: |
* Assemble the F2 stage. | |
Line 28: | Line 58: |
*Manufacturing test(Solder reflow process) *The Power unit(substrate) is divided and processed in a reflow oven. There is no problem even though some solder leakage occurs on the upper part surface. *Operational test(Power unit for 4ch WDS main box) *Continuous operation for 6 hours at twice normal load(334mA). Representation temperature of component surface(upper part) is 51℃(at room temp. 22℃). -->no problem. |
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Line 29: | Line 66: |
*Operational test(for power unit) acquisition and analysis of thermal data. *Main board(WDS main PCB) mounting and implementation. |
Agenda/Minutes of the VIS Meeting on 2017/3/24
2017/3/24 13:30 -
Participants:
Progress report
Type-A (Takahashi)
Past week report
Installation in Y-end:
13th(Mon)
- Assembled cables for PCV for the BF damper.
- Started cabling between the BF and the F3.
14th(Tue)
- Continued cabling between the BF and the F3.
- All cables reached the EQ stop for F3.
15th(Wed)
- Tuned the F3 after cabling.
- The effective weight of cables was about 1kg. It was larger than our prediction.
- Removed the ballast mass inside the BF.
16th(Thu)
- Repaired the stepping motor driver and modified the release sensor monitor.
17th(Fri)
- Assembled the end plate for F2.
21st(Tue)
- Calibrated the LVDT of F3 using the digital system.
- The keystone of BF was not working.
22nd(Wed)
- Took the F2 from the box and moved it into the clean booth.
- Lifted up the DP stage and adjusted the weight of DP.
23rd(Thu)
- Lifted down the BF stage into the corrugate tube.
- The position of keystone on the F3 was too high.
- The cable cramp on the bottom of BF was hitting the release sensor.
- Adjusted the yaw rotation of BF.
Plan for coming weeks
- Assemble the F2 stage.
Type B (Mark)
Past week report
Plan for coming weeks
Type-Bp (Shoda)
Past week report
Plan for coming weeks
IMMT (Ohishi)
Past week report
Plan for coming weeks
Watchdog system (Tanaka)
Past week report
- Manufacturing test(Solder reflow process)
- The Power unit(substrate) is divided and processed in a reflow oven.
- There is no problem even though some solder leakage occurs on the upper part surface.
- The Power unit(substrate) is divided and processed in a reflow oven.
- Operational test(Power unit for 4ch WDS main box)
- Continuous operation for 6 hours at twice normal load(334mA).
Representation temperature of component surface(upper part) is 51℃(at room temp. 22℃). -->no problem.
- Continuous operation for 6 hours at twice normal load(334mA).
Plan for coming weeks
- Operational test(for power unit) acquisition and analysis of thermal data.
- Main board(WDS main PCB) mounting and implementation.
Safety
- Incidents:
- Foreseen risks
- Type-A:
- Type-B:
- Type-Bp:
Discussion
Travel Plans
- Travel (Week of 3/27):
- Takahashi:
- Shoda:
- Mark:
- Fabian:
- Okutomi:
- Fujii:
- Ishizaki:
- Hirata:
- Sato:
- Enzo:
- Hashimoto (Hosei Univ.):
- Ohishi:
- Tanaka:
- Perry:
- Travel (Week of 4/3):
- Takahashi:
- Shoda:
- Mark:
- Fabian:
- Okutomi:
- Fujii:
- Ishizaki:
- Hirata:
- Sato:
- Enzo:
- Hashimoto (Hosei Univ.):
- Ohishi:
- Tanaka:
Next meeting
On 2017/3/31(Fri)